Just the the update earlier this evening and started a test print, and now I'm experiencing the same step timing issue as mentioned above.
D3 Mini with 1LC in standalone mode.
There printer is currently halted with this error message:
30.8.2024, 18:29:54 Error: Movement halted because a step timing error occurred (code 3). Please reset the controller.
30.8.2024, 17:55:27 ABS filament loaded
ABS filament loaded & config applied
30.8.2024, 17:54:49 16 points probed, min error -0.030, max error 0.016, mean -0.012, deviation 0.013
Height map saved to file 0:/sys/heightmap.csv
Height map saved to file 0:/sys/adaptive_heightmap.csv
30.8.2024, 17:54:18 Default grid: X10.0:340.0, Y10.0:340.0, Number of points: X12 Y12, 144 points
Adaptive grid: X120.833:229.167, Y120.833:229.136, Number of points: X4 Y4, 16 points
30.8.2024, 17:53:57 M32 "0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode"
File 0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode selected for printing
This is the M122 outputs:
30.8.2024, 20:23:58 M122
=== Diagnostics ===
RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode)
Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ
Used output buffers: 11 of 40 (37 max)
=== RTOS ===
Static ram: 92328
Dynamic ram: 95720 of which 0 recycled
Never used RAM 45628, free system stack 126 words
Tasks: NETWORK(1,ready,19.3%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.0%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,794) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,339) MAIN(1,running,77.6%,627) IDLE(0,ready,1.4%,29) AIN(4,delaying,0.8%,259), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 02:41:46 ago, cause: software
Last software reset at 2024-08-30 17:42, reason: User, Gcodes spinning, available RAM 52612, slot 0
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
Aux0 errors 0,0,0
MCU temperature: min 45.7, current 46.0, max 46.0
Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/916/440, gc cycles 2170
Events: 0 queued, 0 completed
Date/time: 2024-08-30 20:23:53
Slowest loop: 46.99ms; fastest: 0.13ms
=== Storage ===
Free file entries: 17
SD card 0 detected, interface speed: 22.5MBytes/sec
SD card longest read time 5.7ms, write time 7.2ms, max retries 0
=== Move ===
Segments created 178, maxWait 0ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/39.68ms), max steps late 0, ebfmin 0.00, ebfmax 0.00
Pos req/act/dcf: -3086.00/-3086/0.45 -23971.00/-23971/0.43 33160.00/33160/-0.00
no step interrupt scheduled
Driver 0: standstill, SG min 8, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 2: standstill, SG min 2, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 4: standstill, SG min 2, read errors 0, write errors 0, ifcnt 23, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 5: not present
Driver 6: not present
=== DDARing 0 ===
Scheduled moves 66586, completed 66560, LaErrors 0, Underruns [0, 0, 0]
=== DDARing 1 ===
Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
=== Heat ===
Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
Heater 0 is on, I-accum = 0.4
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Movement locks held by null, null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is doing "G1 X192.529 Y130.297 E.90485" in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is doing "G4 P250" in state(s) 0 0, running macro
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
File2 is idle in state(s) 0
Queue2 is idle in state(s) 0
Q0 segments left 1, axes/extruders owned 0x0000807
Code queue 0 is empty
Q1 segments left 0, axes/extruders owned 0x0000000
Code queue 1 is empty
=== Filament sensors ===
check 0 clear 0
Extruder 0 sensor: no filament
=== CAN ===
Messages queued 247, received 600, lost 0, ignored 0, errs 0, boc 0
Longest wait 6ms for reply type 6024, peak Tx sync delay 132, free buffers 26 (min 25), ts 128/128/0
Tx timeouts 0,0,0,0,0,0
=== Network ===
Slowest loop: 20.21ms; fastest: 0.07ms
Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
HTTP sessions: 1 of 8
=== WiFi ===
Interface state: active
Module is connected to access point
Failed messages: pending 0, notrdy 0, noresp 0
Firmware version 2.1.0
MAC address c4:5b:be:ce:91:93
Module reset reason: Power up, Vcc 3.37, flash size 2097152, free heap 43044
WiFi IP address 192.168.30.50
Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0
Clock register 00002001
Socket states: 0 0 0 0 0 0 0 0
30.8.2024, 20:23:54 M122 B121
Diagnostics for board 121:
Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4+3 (2024-08-28 11:24:12)
Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
All averaging filters OK
Never used RAM 6672, free system stack 79 words
Tasks: Move(3,nWait 7,0.0%,84) TMC(2,delaying,3.6%,52) HEAT(2,nWait 6,0.4%,88) CanAsync(5,nWait 4,0.0%,48) CanRecv(3,nWait 1,0.0%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,91.0%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0%
Owned mutexes:
Last reset 02:41:43 ago, cause: power up
Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0
Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok
Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0
Moves scheduled 65223, hiccups 0 (39.68/39.68ms), segs 58, step errors 0 (types 0x0), maxLate 0 maxPrep 0, ebfmin 0.00 max 0.00
Peak sync jitter -1/8, peak Rx sync delay 199, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3459548387 ticks, disabled
VIN voltage: min 24.5, current 24.5, max 24.6
MCU temperature: min 41.1C, current 75.3C, max 75.5C
Driver 0: pos 2824553, 568.8 steps/mm, standstill, SG min 2, read errors 0, write errors 0, ifcnt 12, reads 9061, writes 0, timeouts 0, DMA errors 0, CC errors 0
Last sensors broadcast 0x00000012 found 2 164 ticks ago, 0 ordering errs, loop time 0
CAN messages queued 405, send timeouts 0, received 171, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 18, error reg 0
dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
Accelerometer: LIS3DH, status: 00
I2C bus errors 0, naks 0, contentions 0, other errors 0
=== Filament sensors ===
Interrupt 5726621 to 0us, poll 9 to 925us
Driver 0: ok