Error: Probe was not triggered during probing move
-
Hello, I have this problem when I want to use G32 or G29 command.
When G32 it check 3 defined point end than stop and it show me this error "G32
Error: Probe was not triggered during probing move
Error: Compensation or calibration cancelled due to probing errors".When G29 common it check 2 points and then stop and show me this error.
Could you help me what could be wrong?
I have tried stable release and also the newest rc release of firmware.
I have BLTouch instaled. It looks work well (stop bed when triggered), but when triggered it should show Z-probe value as 1000, but I have always 0. -
if the tilt of your bed is to big. the probing will fail.
level your bed on the 4 corner manually so that its fairly flat. then try again.
-
@veti I have 3 independent z motor configuration. I thought than G32 command should auto level the bed, without manual bed leveling.
-
@milan-baca said in Error: Probe was not triggered during probing move:
I have BLTouch instaled. It looks work well (stop bed when triggered), but when triggered it should show Z-probe value as 1000, but I have always 0.
The value can be very hard to catch on the DWC view because the bltouch triggers and resets again instantly. It doesn't stay triggered.
Can you post your homeall.g as well?
Also the results of M122 and M98 P"config.g" please. -
-
CoreXY certainly does. How are you trying to do the auto calibration?
G32 calls bed.g
https://duet3d.dozuki.com/Wiki/Bed_levelling_using_multiple_independent_Z_motors
Can you post your homeall.g as well?
Also the results of M122 and M98 P"config.g" please. -
M122
=== Diagnostics ===
RepRapFirmware for Duet 3 MB6HC version 3.3RC3 (2021-05-26 12:29:42) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
Board ID: 08DJM-956BA-NA3TJ-6J9FJ-3S86R-1T96T
Used output buffers: 1 of 40 (13 max)
=== RTOS ===
Static ram: 150784
Dynamic ram: 62052 of which 160 recycled
Never used RAM 141196, free system stack 126 words
Tasks: SBC(ready,5.2%,338) HEAT(delaying,0.0%,295) Move(notifyWait,0.0%,275) CanReceiv(notifyWait,0.0%,945) CanSender(notifyWait,0.0%,360) CanClock(delaying,0.0%,333) TMC(notifyWait,7.9%,59) MAIN(running,86.8%,922) IDLE(ready,0.0%,29), total 100.0%
Owned mutexes: HTTP(MAIN)
=== Platform ===
Last reset 00:38:42 ago, cause: software
Last software reset at 2021-06-13 15:27, reason: User, none spinning, available RAM 141196, slot 1
Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
Error status: 0x00
Aux0 errors 0,0,0
Aux1 errors 0,0,0
Step timer max interval 133
MCU temperature: min 39.4, current 39.6, max 53.4
Supply voltage: min 23.9, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
12V rail voltage: min 12.0, current 12.0, max 12.1, under voltage events: 0
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Driver 0: position 66722, standstill, reads 27175, writes 23 timeouts 0, SG min/max 0/227
Driver 1: position -24410, standstill, reads 27175, writes 23 timeouts 0, SG min/max 0/227
Driver 2: position 28000, standstill, reads 27184, writes 14 timeouts 0, SG min/max 0/0
Driver 3: position 0, standstill, reads 27176, writes 22 timeouts 0, SG min/max 0/228
Driver 4: position 0, standstill, reads 27176, writes 22 timeouts 0, SG min/max 0/233
Driver 5: position 0, standstill, reads 27177, writes 22 timeouts 0, SG min/max 0/246
Date/time: 2021-06-13 16:06:00
Slowest loop: 177.37ms; fastest: 0.03ms
=== Storage ===
Free file entries: 10
SD card 0 not detected, interface speed: 37.5MBytes/sec
SD card longest read time 0.0ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 125, maxWait 297675ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 43, completed moves 43, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP* is doing "M122" in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger* is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== CAN ===
Messages queued 20904, send timeouts 20901, received 0, lost 0, longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 49 (min 49), ts 11614/0/0
Last cancelled message type 30 dest 127
=== SBC interface ===
State: 4, failed transfers: 0
Last transfer: 1ms ago
RX/TX seq numbers: 16462/16462
SPI underruns 0, overruns 0
Number of disconnects: 0, IAP RAM available 0x2c8bc
Buffer RX/TX: 0/0-0
=== Duet Control Server ===
Duet Control Server v3.3-rc3
Code buffer space: 4096
Configured SPI speed: 8000000 Hz
Full transfers per second: 35.35
Codes per second: 0.09
Maximum length of RX/TX data transfers: 2756/864M98 P"config.g"
Error: M350: Driver 3 does not support x0 microstepping with interpolation
Driver 4 does not support x0 microstepping with interpolation
Driver 5 does not support x0 microstepping with interpolation
Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
Warning: M307: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 516C -
@milan-baca said in Error: Probe was not triggered during probing move:
Error: M350: Driver 3 does not support x0 microstepping with interpolation
Driver 4 does not support x0 microstepping with interpolation
Driver 5 does not support x0 microstepping with interpolationThose are your Z drivers, correct? Have you changed microstepping since posting your config.g above?
-
Remove this from your homeall
G92 Z0 ; set Z position to axis minimum (you may want to adjust this)
-
@phaedrux yes I change it to
M350 X16 Y16 Z16:16:16 E16 I1I change it back to Z16 and now
M98 P"config.g"
Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
Warning: M307: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 516C -
@phaedrux
I removed G92 Z0 from homeall.gbut still same error
-
Reduce your dive height from M558 H15 to H5
-
@phaedrux not helped, Error: This kinematics does not support auto-calibration is still there
-
@milan-baca I think you must have made another change to config.g. Please post it as it is now.
-
-
easier to read
; Configuration file for Duet 3 (firmware version 3) ; executed by the firmware on start-up ; ; generated by RepRapFirmware Configuration Tool v3.2.3 on Sun Apr 04 2021 22:18:55 GMT+0200 (CEST) ; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Duet 3" ; set printer name M669 K1 ; select CoreXY mode M912 S-13.7 ; mcu temperature correction ; Drives M569 P0.0 S0 ;H50 V50 D3 ; physical drive 0.0 goes forwards axis X M569 P0.1 S0 ;H50 V50 D3 ; physical drive 0.1 goes forwards axis Y M569 P0.2 S0 ; physical drive 0.2 goes forwards EXTRUDER M569 P0.3 S0 ;H50 V50 D3 ; physical drive 0.3 goes forwards M569 P0.4 S0 ;H50 V50 D3 ; physical drive 0.3 goes forwards M569 P0.5 S0 ;H50 V50 D3 ; physical drive 0.3 goes forwards M584 X0.0 Y0.1 Z0.3:0.4:0.5 E0.2 ; set drive mapping M671 X-26,188:155,021:331,23 Y-20,717:307,493:-20,717 S50 ;Z Lift Point position M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation M92 X160.00 Y160.00 Z1600.00 E712.00 ; set steps per mm M566 X1200.00 Y1200.00 Z30.00 E120.00 ; set maximum instantaneous speed changes (mm/min) M203 X18000.00 Y18000.00 Z1800.00 E1200.00 ; set maximum speeds (mm/min) M201 X1600.00 Y1600.00 Z100.00 E250.00 ; set accelerations (mm/s^2) M906 X1400 Y1400 Z1400 E300 I30 ; set motor currents (mA) and motor idle factor in per cent M84 S30 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X320 Y320 Z321 S0 ; set axis maxima ; Endstops M574 X1 S1 P"io0.in" ; configure active-high endstop for low end on X via pin io0.in M574 Y1 S1 P"io1.in" ; configure active-high endstop for low end on Y via pin io1.in ; Z-Probe M950 S0 C"io7.out" ; create servo pin 0 for BLTouch M558 P9 C"io7.in" H15 F150 T6000 R0.2 A5 G31 P25 X22.775 Y5.21 Z2.5 ; set Z probe trigger value, offset and trigger height M557 X25:282 Y10:282 P5:5 ; define mesh grid ; Heaters M308 S0 P"temp0" Y"thermistor" T100000 B4267 ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0 M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M308 S1 P"temp1" Y"thermistor" T100000 B3950 ; configure sensor 1 as thermistor on pin temp1 M950 H1 C"out1" T1 ; create nozzle heater output on out1 and map it to sensor 1 M307 H1 R3.678 C133.6 D6.67 S1.00 V24.0 M143 H1 S280 ; set temperature limit for heater 1 to 280C ; Fans M950 F0 C"out7" ;Q250 ; create fan 0 on pin out7 and set its frequency M106 P0 S0 H1 T45 ; set fan 0 value. Thermostatic control is turned on M950 F1 C"out4" Q500 ; create fan 1 on pin out4 and set its frequency M106 P1 S1 H-1 ; set fan 1 value. Thermostatic control is turned of ; Tools M563 P0 D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined ;M581 Y S1 T2 ; Miscellaneous M308 S10 Y"mcu-temp" A"MCU" M501 M911 S22 R23.5 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss T0
Your M671 doesn't look valid to me
how is your bed supported? what are the co-ordinates of the screws? -
I agree with @jay_s_uk. Change the commas in the M671 command to fullstops.
-
@jay_s_uk
I am using calculator from this project
https://miragec79.github.io/HevORT/firmwaresettings.html -
@dc42 thank you very much guys problem was in M671 command in numbers
I look at it many times but after you point to that command I saw the problem. It was decimal separator in coordinates
-
@dc42
G32 command now work wellstill have a problem with G29
after few points I got
Error: Probe already triggered before probing move startedps: should I make a new thread or can I continue here?