Problem with Fan Settings Across 3HC and Mini 5+
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I am testing 2 fans and having strange trouble. I cant get the config.g setup properly.
I have a 4 pin PWM fan connected to a Duet 3 Mini 5+ monitoring sensor 15, and i have another 4 pin PWM fan connected to a 3HC monitoring sensor 16. both 15 and 16 are a thermocouple board on the mainboard.
the strange thing is that if i set either of these to monitor H4, the fans work just fine and turn on when proper temperature is reached.
works fine
M950 F3 C"!out3+out3.tach" Q500 ; ; Chamber Heater Fan Noctua NF-F12 Industrial M106 P3 C"Chamber Heater Fan" H15 T30 ; S0.3 L0.3 X0.6 B0.1 T30:40 ; set fan 1 name and value. Thermostatic control turned on for Hotend.
does not work, fan runs 100% continuously
M950 F9 C"!1.out4+out4.tach" Q25000 ;Q500 4028 filter fan ; create fan 0 on pin out4 and set its frequency M106 P9 C"Testing Chamber Fan" H16 T30
however if i set to monitor sensor 4, they work as expected.
M950 F9 C"!1.out4+out4.tach" Q25000 ;Q500 4028 filter fan ; create fan 0 on pin out4 and set its frequency M106 P9 C"Testing Chamber Fan" H4 T30
i'm confused. even though these are being shared across CAN bus, it sometimes works and sometimes does not.
config.g
; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"V-Core3" ; set printer name M669 K11 Y1:-1:0:-1 ; Dual Markforged Kinematics https://forum.duet3d.com/topic/7796/haq-xy/125 https://forum.duet3d.com/topic/21021/dual-markforged-kinematics?_=1672244913067 ;M669 K1 X1:0:0:0 Y1:-1:0:-1 Z0:0:1:0 U0:0:0:1; Matrix mapping for Axis - X:Y:Z:U G21 ; Set Units to Millimeters ; Network M552 S2 ; enable network, note P0.0.0.0 sets auto DHCP M553 P255.255.255.0 ; set subnet mask M554 P192.168.1.20 ; set gateway M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet G4 S2 ; wait for expansion boards to start ; Drives M569 P0.0 S0 D2 ; Left Z physical drive 0.0 goes forwards M569 P0.1 S0 D2 ; Rear Z physical drive 0.1 goes forwards M569 P0.2 S0 D2 ; Right Z physical drive 0.2 goes forwards M569 P0.3 S1 D2 ; Right U toolhead drive 0.3 goes forwards M569 P0.4 S1 D2 ; Left X toolhead drive 0.4 goes forwards M569 P0.5 S0 D2 ; Left Y drive 0.5 goes forwards M569 P0.6 S1 D2 ; Right Y drive 0.6 goes reverse M569 P20.0 S1 D2 ; Extruder physical drive 20.0 goes forwards Toolboard 1LC M569 P21.0 S1 D2 ; Extruder physical drive 21.0 goes forwards Toolboard 1LC M569 P1.0 S0 D2 ; Extruder physical drive 1.0 goes forwards Expansion 3HC M569 P1.1 S0 D2 ; Extruder physical drive 1.1 goes forwards Expansion 3HC M569 P1.2 S1 D2 ; Extruder physical drive 1.2 goes forwards Expansion 3HC M584 Z0.0:0.1:0.2 Y0.5:0.6 X0.4 U0.3 E20.0:21.0:1.0:1.1 ; set drive mapping M350 U16 X16 Y16 Z16 E16:16:16:16 I1 ; configure microstepping with interpolation M92 U80.0 X80.00 Y80.00 Z800.00 E690:690:690:690 ; set steps per mm M906 U2000 X2000 Y2000 Z1800 E1000:1000:1000:1000 I30 ; set motor currents (mA) and motor idle factor in per cent -- safe for Duet 3 mini 5+ M84 S30 ; Set idle timeout ;M98 P"0:/sys/setspeeds.g" ; Set speed and acceleration M566 U500.00 X500.00 Y500.00 Z60.00 E300:300:300:300 P1 ;E300:300 P1 ;X1500.00 Y1500.00 Z6.00 E300 P1 ;E120.00 P1 ; set maximum instantaneous speed changes (mm/min) M203 U30000.00 X30000.00 Y30000.00 Z1000.00 E7200:7200:7200:7200 ;E7200:3600 ;E3600.00 ; set maximum speeds (mm/min) M201 U10000.00 X10000.00 Y10000.00 Z100.00 E10000:10000:10000:10000 ;E10000:3600 ;E3600.00 ; set accelerations (mm/s^2) M207 S0.6 F7200 Z0.2 ; firmware retraction orbiter 2.0 ; Axis Limits M208 X-70 U0 Y0 Z0 S1 ; set axis minima M208 X300 U380 Y306 Z300 S0 ; X310 ; set axis maxima ;M208 X-70:310 Y0:308 U0:308 Z0:300 ; Endstops M574 X1 S1 P"20.io2.in" ; configure active high endstops Toolhead 1 X low end M574 U2 S1 P"21.io2.in" ; configure active high endstops Toolhead 2 U high end M574 Y2 S1 P"io2.in" ; configure active high endstops Y. IO0 and IO1 also are UART, so do not put endstops on them, use them elsewhere to free up UART. M574 Z1 S2 M671 X-71:155:381 Y-1.5:305:-1.5 S5 ; NEW WIDEBOI WITH EXTRUSION SUPPORT LEADSCREW POSITIONS define positions of Z leadscrews or bed levelling screws ;M671 X-4.5:155:304.5 Y-4.5:305:-4.5 S5 ; OLD NON-WIDEBOI EXTRUION SUPPORT LEADSCREW POSITIONS define positions of Z leadscrews or bed levelling screws ;M557 X30:280 Y20:300 P5 ; define 5x5 mesh grid M557 X30:270 Y20:270 P5 ; Heaters M308 S0 P"temp0" Y"thermistor" T100000 B3950 A"Keenevo 600W Bed" ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 Q10 ; Define Heater0 as the heated bed, bind to Sensor0 M140 H0 P0 ; Define Heated Bed M307 H0 R0.602 K0.401:0.000 D2.44 E1.35 S1.00 B0 ; PID Tuning for Heater0, Heated Bed (100C) M143 H0 S140 T0 A0 ; Set temperature limit for Heater0 to 120C M308 S1 P"20.temp0" Y"thermistor" T100000 B4725 C7.060000e-8 A"Slice Hotend 0" ;Slice Engineering 300C thermistor, settings are online M950 H1 C"20.out0" T1 Q100 ; Define Heater1 as Extruder0 heater, bind to Sensor1 M307 H1 R2.808 K0.368:0.000 D4.56 E1.35 S1.00 B0 V23.8 ; PID Tuning for Heater1, Extruder0 (240C) M143 H1 S325 T1 A0 ; Set temperature limit for heater 1 to 285C M308 S2 P"temp1" Y"thermistor" T100000 B3950 C7.060000e-8 A"Chamber" ; configure sensor 2 as thermistor on pin temp1 M950 H2 C"out1" T2 ;Q10 ; create chamber heater output on out1 and map it to sensor 2 M307 H2 R0.01 K0.200:0.000 D60 E1.35 S1.00 B1 ; enable bang-bang mode for the chamber heater and set PWM limit M141 H2 ; map chamber to heater 2 M143 H2 S120 T2 A0 ; set temperature limit for heater 2 to 60C M308 S3 P"21.temp0" Y"pt1000" A"Slice Hotend 1" ;Slice Engineering RTD PT1000 450C, settings are online M950 H3 C"21.out0" T3 Q100 ; Define Heater1 as Extruder0 heater, bind to Sensor1 M307 H3 R2.808 K0.368:0.000 D4.56 E1.35 S1.00 B0 V23.8 ; PID Tuning for Heater1, Extruder0 (240C) M143 H3 S425 T3 A0 ; S325 ; Set temperature limit for heater 1 to 285C M308 S4 P"20.temp1" Y"thermistor" A"Cooling Block" T100000 B3950 C7.060000e-8 ; Define Sensor as Chamber temperature M308 S5 Y"drivers" A"4028 Power" ; 4028 power using spare heater M308 S6 Y"mcu-temp" A"Mini 5+ MCU" ; Define Sensor3 as the integrated MCU temperature sensor M308 S7 Y"drivers" A"Mini 5+ TMC Drivers" ; Define Sensor4 as the TMC overheat sensor M308 S8 Y"mcu-temp" P"20.dummy" A"Toolboard0 MCU" M308 S9 Y"drivers" P"20.dummy" A"1LC0 Stepper" M308 S10 Y"mcu-temp" P"21.dummy" A"Toolboard1 MCU" M308 S11 Y"drivers" P"21.dummy" A"1LC1 Stepper" M308 S12 Y"mcu-temp" P"1.dummy" A"3HC MCU" M308 S13 Y"drivers" P"1.dummy" A"3HC TMC Drivers" M308 S14 P"temp2" Y"thermistor" T100000 B3950 C7.060000e-8 A"Orbiter Motor" ; configure sensor 9 as thermistor on pin temp2 M308 S15 P"spi.cs1" Y"thermocouple-max31856" K"K" A"TC0 Chamber Heater"; define temperature sensor number 10 as a K Type thermocouple on the first port of a temperature daughter board plugged into the expansion board with CAN bus address 3. M308 S16 P"spi.cs2" Y"thermocouple-max31856" K"K" A"TC1 Chamber Fins"; define temperature sensor number11 as a T Type thermocouple on the first port of a temperature daughter board plugged into the expansion board with CAN bus address 3. ;M308 S17 P"21.temp1" Y"thermistor" T4500000 B5315 C3.219245e-9 A"BLUE MELLOW" ; blue Mellow high temp thermistor (toolboard)https://duet3d.dozuki.com/Wiki/Connecting_thermistors_or_PT1000_temperature_sensors#Section_RepRapFirmware_3_x ;M308 S17 P"21.temp1" Y"pt1000" T500000 B4666 C1.117125e-7 A"WHITE MELLOW" ; white Mellow high temp pt1000 (toolboard)https://duet3d.dozuki.com/Wiki/Connecting_thermistors_or_PT1000_temperature_sensors#Section_RepRapFirmware_3_x ; Fans M950 H4 C"!out2" T2 Q10 ;H2 ; Define Heater2 as the 4028 fan power, bind to Sensor3 M143 H4 P2 S200 A0 ; Needed M143 to set max temp so the graph scaled correctly M950 F0 C"!20.out1+out1.tach" Q25000 ;Q500 ; create fan 0 on pin out4 and set its frequency M106 P0 C"T0 Layer Fan" L0.0 X1.0 S0 H-1 B0.1 ; set fan 0 name and value. Thermostatic control is turned off M950 F1 C"20.out2+out2.tach" Q500 ; Fan 1 uses out3, and using out3.tach as a tacho input M106 P1 C"T0 Hotend Fan" S0 H1 T45 ; For M106 the H is sensor # and NOT heater #. set fan 1 name and value. Thermostatic control turned on for Hotend M950 F2 C"out5" Q500 ; create fan 1 on pin out5 and set its frequency M106 P2 C"Mini 5+ Board Fan" S0 H5:6:7 T45 ; set fan 1 name and value. Thermostatic control turned on for Hotend M950 F3 C"!out3+out3.tach" Q500 ; ; Chamber Heater Fan Noctua NF-F12 Industrial M106 P3 C"Chamber Heater Fan" H15 T30 ; S0.3 L0.3 X0.6 B0.1 T30:40 ; set fan 1 name and value. Thermostatic control turned on for Hotend. M950 F4 C"1.out3" Q500 ; ; out6 on old mini 5+ ; create fan 4 for Water Cooling 12V Fan 4 on pin out4 and set its frequency M106 P4 C"Radiator Cooling Fan" S0 H4 T35 ; set fan 1 name and value. Thermostatic control turned on for liquid cooling hotend M950 F5 C"!out4+out4.tach" Q25000 ;Q500 ; create fan 4 for Water Cooling 12V Fan 4 on pin out4 and set its frequency M106 P5 C"Liquid Cooling Pump" L0.0 X1.0 S0.5 H4 ;S0.0 T20 ; set fan 4 name and value. Thermostatic control turned on for liquid cooling hotend M950 F6 C"!21.out1+out1.tach" Q25000 ;Q500 ; create fan 6 on pin out4 and set its frequency M106 P6 C"T1 Layer Fan" L0.0 X1.0 S0 H-1 B0.1 ; set fan 6 name and value. Thermostatic control is turned off M950 F7 C"21.out2+out2.tach" Q500 ; Fan 7 uses out3, and using out3.tach as a tacho input M106 P7 C"T1 Hotend Fan" S0 H3 T45 ; set fan 7 name and value. Thermostatic control turned on for Hotend M950 F8 C"1.out6" Q500 ; create fan 1 on pin out5 and set its frequency M106 P8 C"3HC Board Fan" S0 H12:13 T45 ; set fan 1 name and value. Thermostatic control turned on for Hotend M950 F9 C"!1.out4+out4.tach" Q25000 ;Q500 4028 filter fan ; create fan 0 on pin out4 and set its frequency M106 P9 C"Testing Chamber Fan" H16 T30 ; Tool 0 X Axis M563 P0 D0 H1 X0 F0 S"Mosquito Mag Liquid" ; define tool 0 G10 P0 X0 Y0 Z-0.54 ; Z-0.54 S210 R175 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M568 P0 S210 R175 ; Tool 1 U Axis M563 P1 D1 H3 X3 F6 S"Mosquito Mag Air" ; define tool 0 G10 P1 U0 X0 Y0 Z0 ; S210 R175 ; L1 ; set tool 1 axis offsets, set initial tool 1 active 60C and standby temperatures to 0C M568 P1 S210 R175 ; Tool 2-- Toolhead 2 with ROME 1 M563 P2 D1:2 H3 X3 F6 S"ROME 1" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans G10 P2 U-2.31 X0 Y0.44 Z0.00 ; Z0.04 S210 R175 ; L1 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M567 P2 E1:1 ; set mix ratio 100% on both extruders for copy mode M568 P2 S210 R175 ; Tool 3-- Toolhead 2 with ROME 2 M563 P3 D1:3 H3 X3 F6 S"ROME 2" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans G10 P3 U-2.31 X0 Y0.44 Z0.00 ; Z0.04 S210 R175 ; L1 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M567 P3 E1:1 ; set mix ratio 100% on both extruders for copy mode M568 P3 S210 R175 ; Tool 4-- copy mode ;M563 P4 D0:1 H1:3 X0:3 F0:6 S"copy mode" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans ;G10 P4 U-77.5 X77.5 Y0 S210 R175 ; set tool offsets and temperatures for tool 2 ;M567 P4 E1:1 ; set mix ratio 100% on both extruders for copy mode ; Tool 5-- mirror mode ;M563 P5 D0:1 H1:3 X0:3 F0:6 S"mirror mode" ; tool for mirror mode ;G10 P5 U-77.5 X77.5 Y0 S210 R175 ; tool offset for mirror mode (flipped X offset) ;M567 P5 E1:1 ; set mix ratio 100% on both extruders for mirror mode ; Z-Probe Euclid Probe ;M558 P5 C"20.io0.in" H5 F400 T5000 ; set Z probe type to unmodulated and the dive height + speeds M558 P8 C"^20.io0.in" H8 F400 T9000 A1 ; S0.01 ; set Z probe type to unmodulated and the dive height + speeds G31 P1000 X-28 Y-20 Z9.71 ; Z9.21 ; K0 ; set Z probe trigger value, offset and trigger height, more Z means closer to the bed ;; BLTouch ; M950 S0 C"io7.out" ; Create a servo pin on io7 ; M558 P9 C"io7.in" H5 F240 T10800 A5 ; set Z probe type to unmodulated and the dive height + speeds ; G31 P25 X-28.00 Y-13.00 Z0.78 ; set Z probe trigger value, offset and trigger height, more Z means closer to the bed ;Accelerometer M955 P20.0 I14 ;Input Shaper M593 P"zvdd" F31 ; for 10k acceleration ;M593 P"mzv" F42.5 ; for 15k acceleration ;Filament Sensor0 ;M591 D0 P3 C"20.io1.in" S1 ;M591 D0 L27 R10:190 ;ROME Filament Sensor0 ;M591 D2 P1 C"21.io0.in" S1 ;M591 D2 L27 R10:190 ;M574 U2 S1 P"21.io0.in" ; configure active high endstops Toolhead 2 ROME toolhead filament sensor ;M577 wait until endstop is triggered. Does equivalent exist for a general IO sensor? M950 J0 C"^!21.io0.in" ;PanelDue 5i M575 P1 S1 B57600 ;NeoPixels x3 M150 X3 Q4000000 ;R128 U128 B128 P128 S2 F0 M150 X3 R255 U255 B255 W255 P255 S2 F0 ; display led ; Custom settings G29 S1 M572 D0:1 S0.065 ; set Pressure Advance K-factor M501 M376 H3 ;M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss global daemonLoop = true ; init filament sensor error global variables if !exists(global.filamentTimestamp) global filamentCounter = 0 global filamentTimestamp = state.Uptime ; init print time logging if !exists(global.runtime) M98 P"runtime.g" ; init LED variables if !exists(global.warmUp) global warmUp = false ; Select default tool M404 N1.75 ; Define filament diameter for print monitor T0
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Can you send M98 P"config.g" and see if any errors are generated?
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@Phaedrux i dont see any related errors. i have to resolve my Daemon issue.
M98"config.g"
5/25/2023, 12:20:47 PM Error: bad model parameters Accelerometer 20:0 type LIS3DH with orientation 14 samples at 1344Hz with 10-bit resolution Warning: the height map was loaded when the current Z=0 datum was not determined by probing. This may result in a height offset. Warning: Macro file config-override.g not found Error: in file macro line 219 column 20: meta command: variable 'daemonLoop' already exists
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@RogerPodacter to add more details, if i physcally swap the 2 fans, the 3HC continues to run 100%. so the fans hardware are ok, its something wrong with the configuration or the sensor number assignments etc. whichever fan is on the 3HC, that one doesnt work.
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What's the can address on the 3HC? 1?
Can you send M122 and M122 B1 and report the results here?
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@Phaedrux yes the 3HC is address 1 default.
Mainboard M122
5/26/2023, 6:14:09 AM M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.4.2 (2022-09-13 15:14:33) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: J6RFD-NR6KL-K65J0-409NN-LK02Z-7M5YU Used output buffers: 1 of 40 (34 max) === RTOS === Static ram: 103684 Dynamic ram: 113580 of which 308 recycled Never used RAM 21284, free system stack 174 words Tasks: NETWORK(notifyWait,64.4%,215) HEAT(notifyWait,0.8%,342) Move(notifyWait,0.0%,363) CanReceiv(notifyWait,1.9%,772) CanSender(notifyWait,0.0%,336) CanClock(delaying,0.1%,339) TMC(notifyWait,20.0%,106) MAIN(running,113.0%,419) IDLE(ready,113.1%,30) AIN(delaying,14.7%,263), total 328.2% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 23:39:51 ago, cause: software Last software reset at 2023-05-25 06:33, reason: StuckInSpinLoop, GCodes spinning, available RAM 21204, slot 1 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044f80f BFAR 0xe000ed38 SP 0x20003df4 Task MAIN Freestk 771 ok Stack: 0009159f 00090b7c 61070000 421d8000 409b5800 369dc3a0 426ff5c3 42adf895 3b34e113 3b4ba16c 3a03b8df b9fd72b5 3f800002 00000005 00000000 00000000 00000000 00000000 3f800000 20000010 00090b65 421d8000 ffffffff 00000000 00057376 42adf895 2002a654 Error status: 0x00 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 85192032, completed 85192032, timed out 0, errs 0 Step timer max interval 1487 MCU temperature: min 38.1, current 39.8, max 40.9 Supply voltage: min 23.9, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/2, heap memory allocated/used/recyclable 2048/648/616, gc cycles 106635 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11370, writes 48, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11370, writes 48, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11368, writes 48, timeouts 1, DMA errors 0, CC errors 0, failedOp 0x01 Driver 3: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11369, writes 48, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11369, writes 48, timeouts 1, DMA errors 0, CC errors 0, failedOp 0x6a Driver 5: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11369, writes 48, timeouts 0, DMA errors 0, CC errors 0 Driver 6: standstill, SG min 0, read errors 0, write errors 1, ifcnt 67, reads 11369, writes 48, timeouts 0, DMA errors 0, CC errors 0 Date/time: 2023-05-26 06:14:07 Cache data hit count 4294967295 Slowest loop: 89.15ms; fastest: 0.09ms === Storage === Free file entries: 9 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 8.4ms, write time 61.5ms, max retries 0 === Move === DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: mesh, comp offset 0.000 === MainDDARing === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters 2 -1 -1 -1, ordering errs 0 === GCodes === Segments left: 0 Movement lock held by null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty === CAN === Messages queued 767731, received 4771867, lost 0, boc 0 Longest wait 7ms for reply type 6013, peak Tx sync delay 392, free buffers 18 (min 17), ts 425959/425958/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 63.60ms; fastest: 0.00ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions HTTP sessions: 1 of 8 = WiFi = Network state is active WiFi module is providing access point Failed messages: pending 0, notready 0, noresp 0 WiFi firmware version 1.27 WiFi MAC address ea:68:e7:e5:63:f4 WiFi Vcc 3.39, reset reason Power up WiFi flash size 2097152, free heap 25248 WiFi IP address 192.168.1.10 Connected clients 1 Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0
3HC M122
5/26/2023, 6:15:11 AM M122 B1 Diagnostics for board 1: Duet EXP3HC rev 1.02 or later firmware version 3.4.2 (2022-09-13 15:05:23) Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10) All averaging filters OK Never used RAM 158256, free system stack 178 words Tasks: Move(notifyWait,0.0%,160) HEAT(notifyWait,0.4%,88) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.3%,82) CanClock(notifyWait,0.1%,71) TMC(notifyWait,14.1%,99) MAIN(running,63.8%,399) IDLE(ready,0.0%,40) AIN(delaying,21.2%,263), total 100.0% Last reset 23:47:12 ago, cause: power up Last software reset data not available Driver 0: pos 0, 690.0 steps/mm,standstill, SG min 0, mspos 8, reads 54219, writes 107 timeouts 0, steps req 0 done 0 Driver 1: pos 0, 690.0 steps/mm,standstill, SG min 0, mspos 8, reads 54219, writes 107 timeouts 0, steps req 0 done 0 Driver 2: pos 0, 80.0 steps/mm,standstill, SG min 0, mspos 8, reads 54300, writes 27 timeouts 0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter -12/13, peak Rx sync delay 183, resyncs 0/1, no step interrupt scheduled VIN voltage: min 21.0, current 24.2, max 29.0 V12 voltage: min 12.3, current 12.3, max 12.3 MCU temperature: min 28.0C, current 32.1C, max 33.9C Last sensors broadcast 0x00003000 found 2 158 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 1370453, send timeouts 0, received 1456049, lost 0, free buffers 37, min 37, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
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@RogerPodacter there must be some conflict with how i have my fans setup. when i change H16 to H4, the fan works just fine. but when using H16 as a sensor monitor, it runs 100%.
if i set both fans to H-1, both work normally and i can manually control them with 0-100 slider bar.
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What is the temperature difference between H4 and H16? Your set temp is only 30c, so if one is higher than the other, it will run faster.
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@Phaedrux both are reading 21.6 and 21.7. these TC's have been in use for many months. the only difference is i have now added a 3HC trying to use the fan. so its definitely a config.g setup issue.
it allows me to use my hand heat to trigger 30C and challenge the fans easily.
to be clear the mode is on or off, so there is no variable temperature gradient. using H4, the fan turns on at 30C. using H15 or H16, the fan runs 100% non-stop.
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@RogerPodacter is it because you’ve defined fan0 as part of tool 4 and 5? I just did a quick scan, so that might be intentional.
Ian
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@RogerPodacter please upgrade to the latest stable firmware, which is 3.4.5, and test again.
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thanks all, unfortunately the issue remains. i've upgrade all components to 3.5.0 beta 3, but it just seems that a fan running from a 3HC wont accept thermocouple sensor from a Mini 5+. i dont know what else it could be. the best i can understand is a thermocouple on the mainboard cannot be used as a sensor monitor for a fan on the 3HC. but thermistors work fine, so its something related to the daughterboard perhaps.
M122
5/27/2023, 7:52:33 AM M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-beta.3 (2023-04-14 11:28:00) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: J6RFD-NR6KL-K65J0-409NN-LK02Z-7M5YU Used output buffers: 13 of 40 (35 max) Error in macro line 77 while starting up: bad model parameters === RTOS === Static ram: 102968 Dynamic ram: 124060 of which 276 recycled Never used RAM 11896, free system stack 186 words Tasks: NETWORK(ready,19.5%,228) HEAT(nWait,0.1%,336) Move(nWait,0.0%,358) CanReceiv(nWait,0.1%,774) CanSender(nWait,0.0%,336) CanClock(delaying,0.0%,350) TMC(delaying,1.2%,108) MAIN(running,72.5%,454) IDLE(ready,5.8%,29) AIN(delaying,0.8%,266), total 100.0% Owned mutexes: === Platform === Last reset 00:03:28 ago, cause: software Last software reset at 2023-05-27 07:49, reason: User, Gcodes spinning, available RAM 12380, slot 2 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 208820, completed 208820, timed out 0, errs 0 MCU temperature: min 38.8, current 39.8, max 40.4 Supply voltage: min 23.9, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/4, heap memory allocated/used/recyclable 2048/1300/1232, gc cycles 273 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, read errors 0, write errors 1, ifcnt 107, reads 18942, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 1, ifcnt 107, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 0, read errors 0, write errors 1, ifcnt 107, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 2, read errors 0, write errors 1, ifcnt 101, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 2, read errors 0, write errors 1, ifcnt 103, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 5: standstill, SG min 2, read errors 0, write errors 1, ifcnt 105, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 6: standstill, SG min 2, read errors 0, write errors 1, ifcnt 105, reads 18941, writes 16, timeouts 0, DMA errors 0, CC errors 0 Date/time: 2023-05-27 07:52:32 Cache data hit count 372944678 Slowest loop: 89.07ms; fastest: 0.10ms === Storage === Free file entries: 19 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 6.2ms, write time 31.4ms, max retries 0 === Move === DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: mesh, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters 2 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === CAN === Messages queued 2014, received 11765, lost 0, boc 0 Longest wait 3ms for reply type 6053, peak Tx sync delay 6, free buffers 18 (min 17), ts 1044/1043/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 47.89ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 1 of 8 = WiFi = Network state is active Module is providing access point Failed messages: pending 0, notready 0, noresp 0 Firmware version 2.1beta4 MAC address ea:68:e7:e5:63:f4 Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 40124 WiFi IP address 192.168.1.10 Connected clients 1 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0
M122 B1
5/27/2023, 7:53:05 AM M122 B1 Diagnostics for board 1: Duet EXP3HC rev 1.02 or later firmware version 3.5.0-beta.3 (2023-04-13 18:42:24) Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10) All averaging filters OK Never used RAM 157516, free system stack 202 words Tasks: Move(nWait,0.0%,162) HEAT(nWait,0.0%,90) CanAsync(nWait,0.0%,63) CanRecv(nWait,0.0%,79) CanClock(nWait,0.0%,70) TMC(nWait,6.1%,105) MAIN(running,92.5%,431) IDLE(ready,0.0%,40) AIN(delaying,1.3%,265), total 100.0% Last reset 00:04:01 ago, cause: software Last software reset data not available Driver 0: pos 0, 690.0 steps/mm,standstill, SG min n/a, mspos 920, reads 21635, writes 23 timeouts 0, steps req 0 done 0 Driver 1: pos 0, 690.0 steps/mm,standstill, SG min n/a, mspos 616, reads 21636, writes 23 timeouts 0, steps req 0 done 0 Driver 2: pos 0, 80.0 steps/mm,standstill, SG min n/a, mspos 8, reads 21647, writes 13 timeouts 0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter -7/9, peak Rx sync delay 183, resyncs 0/0, no timer interrupt scheduled VIN voltage: min 24.2, current 24.3, max 24.3 V12 voltage: min 12.3, current 12.3, max 12.3 MCU temperature: min 32.2C, current 32.4C, max 32.9C Last sensors broadcast 0x00003000 found 2 194 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 3903, send timeouts 0, received 4117, lost 0, free buffers 37, min 37, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
M122 B20
5/27/2023, 7:54:35 AM M122 B20 Diagnostics for board 20: Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-beta.3 (2023-04-13 18:44:05) Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1) All averaging filters OK Never used RAM 5012, free system stack 92 words Tasks: Move(nWait,0.0%,155) HEAT(nWait,0.3%,100) CanAsync(nWait,0.0%,57) CanRecv(nWait,0.0%,76) CanClock(nWait,0.0%,67) ACCEL(nWait,0.0%,53) TMC(delaying,3.0%,57) MAIN(running,91.6%,344) IDLE(ready,0.0%,27) AIN(delaying,4.9%,142), total 100.0% Last reset 00:05:31 ago, cause: software Last software reset data not available Driver 0: pos 0, 690.0 steps/mm,standstill, SG min 14, read errors 0, write errors 1, ifcnt 111, reads 34519, writes 18, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter -3/8, peak Rx sync delay 218, resyncs 0/0, no timer interrupt scheduled VIN voltage: min 24.0, current 24.1, max 24.2 MCU temperature: min 27.8C, current 29.0C, max 29.1C Last sensors broadcast 0x00000312 found 4 15 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 6669, send timeouts 0, received 5659, lost 0, free buffers 37, min 37, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0 Accelerometer: LIS3DH, status: 00 I2C bus errors 0, naks 3, other errors 0
M122 B21
5/27/2023, 7:55:03 AM M122 B21 Diagnostics for board 21: Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-beta.3 (2023-04-13 18:44:05) Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1) All averaging filters OK Never used RAM 5044, free system stack 92 words Tasks: Move(nWait,0.0%,155) HEAT(nWait,0.2%,83) CanAsync(nWait,0.0%,57) CanRecv(nWait,0.0%,76) CanClock(nWait,0.0%,67) ACCEL(nWait,0.0%,53) TMC(delaying,3.0%,57) MAIN(running,91.8%,346) IDLE(ready,0.0%,27) AIN(delaying,4.9%,142), total 100.0% Last reset 00:05:59 ago, cause: software Last software reset data not available Driver 0: pos 0, 690.0 steps/mm,standstill, SG min 2, read errors 0, write errors 1, ifcnt 114, reads 48483, writes 18, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter -3/8, peak Rx sync delay 215, resyncs 0/0, no timer interrupt scheduled VIN voltage: min 24.3, current 24.3, max 24.5 MCU temperature: min 34.7C, current 34.8C, max 35.1C Last sensors broadcast 0x00000c08 found 3 192 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 7222, send timeouts 0, received 6129, lost 0, free buffers 37, min 37, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0 Accelerometer: LIS3DH, status: 00 I2C bus errors 0, naks 3, other errors 0
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@RogerPodacter are you saying that using a thermistor connected to the main board to control a fan connected to the 3HC works, but using a thermocouple connected to the main board via the Duet3D thermocouple daughter board does not?
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@dc42 yes precisely, that is what i thought. but now that i just looked closer, its a bit different. the H4 thermistor which is my "working" example is actually on one of the toolboards 1LC 20.temp1, not on the mainboard as i thought. so it seemed that my H4 thermistor could control a fan on a 3HC or a fan on the mainboard. however now that i am on v3.4.5, it appears that H4 is no longer working for either of them. now i'm very confused or perhaps the underlying code has changed in the new firmware.
i guess just ignore my topic at this point because i am confused. maybe there was a CAN bus thing which allowed the toolboard but not the 3HC to control over CAN bus, but none seem to work now so its ok.
my original intention was to use the daughterboard thermocouples and have TC0 control a fan on the mainboard, and TC1 control a fan on the 3HC.
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@RogerPodacter said in Problem with Fan Settings Across 3HC and Mini 5+:
my original intention was to use the daughterboard thermocouples and have TC0 control a fan on the mainboard, and TC1 control a fan on the 3HC.
That should work, provided all boards are running firmware 3.4.2 or later.