Duet 3 Mini 5+ Error: short-to-ground reported by driver(s)
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With spreadcycle all the time, D2 as in for eg. M569 P0.1 S1 D2
homing just makes it stand still and buzz. I hope I have understood M569 correctly.x16 microstepping (D2 removed and V50 back) makes things better, but the resonance increases as it picks up speed until it detects a false sensor less endstopp. It is like some kind of vibration that counteracts the movement.
Video of homing @ 500 mA https://youtu.be/Kg_PY0-1OhE (works fine)
Video of homing @ 800 mA https://youtu.be/myc5rtT7meU (problems...)
Firmware
M115 FIRMWARE_NAME: RepRapFirmware for Duet 3 Mini 5+ FIRMWARE_VERSION: 3.3 ELECTRONICS: Duet 3 Mini5plus WiFi FIRMWARE_DATE: 2021-06-15 21:46:20
PSU voltage ~24.5
M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.3 (2021-06-15 21:46:11) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: DL70G-S396U-D65J0-40KMW-2303Z-HP9WR Used output buffers: 3 of 40 (25 max) === RTOS === Static ram: 102724 Dynamic ram: 106072 of which 60 recycled Never used RAM 34848, free system stack 136 words Tasks: NETWORK(ready,16.2%,258) HEAT(delaying,0.0%,373) Move(notifyWait,0.1%,305) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,371) CanClock(delaying,0.0%,347) TMC(notifyWait,0.7%,115) MAIN(running,82.1%,426) IDLE(ready,0.1%,29) AIN(delaying,0.8%,264), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 00:03:16 ago, cause: software Last software reset at 2021-07-12 09:11, reason: User, GCodes spinning, available RAM 34848, slot 0 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 196361, completed 196360, timed out 0, errs 0 Step timer max interval 752 MCU temperature: min 25.3, current 26.4, max 27.1 Supply voltage: min 24.2, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0 Driver 0: position 24960, standstill, SG min/max 0/4, read errors 0, write errors 1, ifcnt 35, reads 10306, writes 12, timeouts 0, DMA errors 0 Driver 1: position 960, short-to-ground, standstill, SG min/max 2/336, read errors 0, write errors 1, ifcnt 40, reads 10304, writes 14, timeouts 0, DMA errors 0 Driver 2: position 2700, standstill, SG min/max 0/0, read errors 0, write errors 1, ifcnt 29, reads 10308, writes 9, timeouts 0, DMA errors 0 Driver 3: position 0, short-to-ground, standstill, SG min/max 2/340, read errors 0, write errors 1, ifcnt 39, reads 10303, writes 14, timeouts 0, DMA errors 0 Driver 4: position 0, standstill, SG min/max 0/2, read errors 0, write errors 1, ifcnt 35, reads 10306, writes 12, timeouts 0, DMA errors 0 Driver 5: position 0, assumed not present Driver 6: position 0, assumed not present Date/time: 2021-07-12 09:15:11 Cache data hit count 371153997 Slowest loop: 7.32ms; fastest: 0.10ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 3.2ms, write time 0.0ms, max retries 0 === Move === DMs created 83, maxWait 23259ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 7, completed moves 7, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1, chamberHeaters = -1 -1 Heater 1 is on, I-accum = 0.0 === GCodes === Segments left: 0 Movement lock held by null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 1795, received 2380, lost 0, longest wait 2ms for reply type 6031, peak Tx sync delay 177, free buffers 17 (min 16), ts 982/981/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 10.80ms; fastest: 0.00ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions HTTP sessions: 1 of 8 - WiFi - Network state is active WiFi module is connected to access point Failed messages: pending 0, notready 0, noresp 0 WiFi firmware version 1.26 WiFi MAC address f0:08:d1:02:ef:4b WiFi Vcc 3.41, reset reason Power up WiFi flash size 2097152, free heap 26664 WiFi IP address 192.168.0.117 WiFi signal strength -51dBm, mode 802.11n, reconnections 0, sleep mode modem Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0
M98 P"config.g" HTTP is enabled on port 80 FTP is disabled TELNET is disabled Accelerometer 121:0 with orientation 16 samples at 1344Hz with 12-bit resolution Warning: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 827C
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What are the specs of the motors? Do they have high back emf by chance?
Also take a look at this page.
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Check your motor winding specs on the manufacturer page. I had the same problem. Bought LDO steppers but the harness came from somewhere else. I just released the pins from the plug on the stepper side and reconfigured them correctly according to the manufacturers diagram.
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@tony449777 If your experience should apply in thiss case the pin out for the stepper motors has to differ between the duet WiFi and the mini 5. Which I highly doubt.
(Away from printer will investigate more when I get hold of stepper motor model no)
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@fotomas It wasn’t the pin out of the driver that was wrong. It was how the output of the driver was actually connected to the coils of the motor. They were physically in the motor plug in the wrong configuration.
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@tony449777 said in Duet 3 Mini 5+ Error: short-to-ground reported by driver(s):
@fotomas It wasn’t the pin out of the driver that was wrong. It was how the output of the driver was actually connected to the coils of the motor. They were physically in the motor plug in the wrong configuration.
This is a common issue because different manufacturers of stepper motors use different pinouts. When using motors with a built-in socket and separate cable, ALWAYS check the phases.
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@dc42 Exactly. That’s what I’m trying to say,
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@tony449777 said in Duet 3 Mini 5+ Error: short-to-ground reported by driver(s):
Check your motor winding specs on the manufacturer page. I had the same problem. Bought LDO steppers but the harness came from somewhere else. I just released the pins from the plug on the stepper side and reconfigured them correctly according to the manufacturers diagram.
If this were the case here and the phases not paired correctly there would be no movement at all, but if you want the videos it's clear there is motion, but at a certain speed there is a lot of vibration and noise.
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I got things working.
I checked wiring, everything was ok (as exprected since wiring was not modified since working ok on a Duet Wifi)
I increased the acceleration (M201) on X/Y from 300 to 800 this made it possible to increase the motor currents on X/Y to 800.
As an effect of this I had to tweak the sensorless homing to use less current.
So increased acceleration seems to be the solution, the problem may still be there but pushed out of bounds for my usage/speeds by increased acceleration.
I do not understand how increased acceleration have effected things. Maybe someone can explain this? It would be nice to know if I run into more trouble.
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That's an interesting result. I don't understand why higher acceleration would solve it either. You've made the motor/stepper combo happy at least.