How to reduce the speed of extrusion
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one extruder on P3
==> M569 P3 S0
please help me ... M584 E????
just send or on config.g ? -
@frafa said in How to reduce the speed of extrusion:
????
M584 E3
Send it to test it, put it in config.g to make it permanent.
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Thank's
Same error on console: M350: Drive E8 does not support 1x microstepping
ok on 16 microstep
but dont works on 1x motor vibrate and dont turn...
Motor: Nema 8 reduct 19:1
leadscrew - M6 metric (1mm per rotation)ok (16 microstep)
M92 ... E60800 ;
M350 E16 I0 ;
M584 E3;ko (full step)
M92 ... E3200 ;
M350 E1 I0 ;
M584 E3;Firmware Name: RepRapFirmware for Duet 2 WiFi/Ethernet
Firmware Electronics: Duet WiFi 1.02 or later
Firmware Version: 1.21RC3 (2018-02-28 build 4)
WiFi Server Version: 1.21RC4(08b3)
Web Interface Version: 1.21-RC4 -
The M584 E3 command must come before the M350 E1 I0.
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ok
M584 E3 before M350
test 16x ok
1x 2x 4x 8x ko, motor vibrate, and do not turn
no error on console ... -
@frafa said in How to reduce the speed of extrusion:
ok
M584 E3 before M350
test 16x ok
1x 2x 4x 8x ko, motor vibrate, and do not turn
no error on console ...That sounds like you have the steps/mm set too high at x8 and below, or the acceleration (M201) set too high. Please confirm that you still have the M92 command before the M350 command, so that the steps/mm will be adjusted automatically.
I still think that it would be much better to make your steps/mm be the steps per mm extrusion from the nozzle, not the steps per mm movement of the plunger.
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Humm....
I tested a lot of steps by decreasing number of steps per mm without success
motor vibrates and does not turn
I only get there in 16x ...order used:
M92 ... E3200 ;
M566 ... E30 ; Set maximum instantaneous speed changes (mm/min) (jerk)
M203 ... E60 ; Set maximum speeds (mm/min)
M201 ... E5 ; Set accelerations (mm/s^2)
M906 ... E550 I60 ;
M584 E3; assign extrude on motor (P3)
M350 E1 I0 ; -
On my list to test.
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Ok thanks
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I'm sorry, I can't reproduce this issue. I used the settings you posted above, then sent G1 E1 first with x16 microstepping. Then I sent M350 to change the microstepping to 8, then 2, then 1 and repeated the G1 E1 command in each case. The motor moved the same amount every time, but was much noisier with lower microstepping.
I am using the candidate firmware build for 2.02RC4, but I don't think there have been any changes that would account for the problem going away. But I suggest you try upgrading to 2.02RC4 anyway when I release it.