Duet 3 Mini noisy StealthChop + no sensorless homing
-
to disable hybrid mode set V to 0
-
Looks like it should be staying in stealthchop for the homing move.
Things you might try...
- Lower the X and Y current before the homing move. You also don't seem to ever be restoring the current back to 100%.
- What happens if you set a very low stall threshold with something like M915 X S-63 F0 H200 R0, do the motors stall then?
-
@Argo said in Duet 3 Mini noisy StealthChop + no sensorless homing:
M92 X200.00 Y200.00 Z400.00 E415.00 ; Set steps per mm
if you have 1.8 degree stepper this should be X100 Y100
-
Ah I lowered the currents for testings. Normally I set them back to 100%.
I'll try lower settings now.@Veti
My bad, thanks for pointing that out. I had 0.9 motors in my Duet Wifi. Argh -
@Argo
do you where running twice the speed. thats where the noise could have come from -
Thank you guys again
With the beta version from the Dropbox archive + correct steps settings and lower sensitivity + no hybrid mode, it's working now and the motors are really quiet.
-
the real beta 1 is here
https://github.com/Duet3D/RepRapFirmware/releases/tag/3.3beta1
not on dropbox -
Are those versions the same? dc42 posted in the thread you linked that it's an unofficial beta build. Idk if he means not for public or it's just because it's a beta.
-
3.3 beta 1 was release 12 days ago.
the dropbox link was from 21.january.if its not in beta 1 then that would be good to know, in case he forgot to merge the bugfix.
-
The bug fix is in the official 3.3beta1 release. The builds currently on Dropbox are later.
-
@dc42
its not in the changelog -
@Veti said in Duet 3 Mini noisy StealthChop + no sensorless homing:
@dc42
its not in the changelogThanks for pointing this out. It is now.