Error when setting up independent motor bed levelling on CoreXY
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No change.
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
No change.
As a test reboot your printer and enter that command (G1 Z5 H2 F420) in the DWC Console, just to be sure it is generating the "not homed" error.
Thanks.
Frederick
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
is there a resource I can follow about the recommended sequence of gcode and/or what are good practices when setting up firmware
Every gcode is documented here: https://duet3d.dozuki.com/Wiki/Gcode#main
It's a good idea to check the relevant gcodes when trouble shooting.
@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
I've put the ;Independent motors leveling section right after the drivers assigning part of config.g and it has made no difference.
How is your config.g laid out now? Can you post it again? The M584 should be above the M350.
The homing file you've posted is from the /system folder right?
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@fcwilt When I start with (G1 Z5 H2 F420) as per your suggestions I get a little but further, namely to G1 X5 Y5 F600 (line 8 in homeall.g) and I get the same error (Error: G0/G1: insufficient axes homed).
@Phaedrux The current config.g:
; General preferences G90 ; Send absolute coordinates... M83 ; ...but relative extruder moves M667 S1 ; Select CoreXY mode ; Network M550 PPrinter Extrusions ;machine name M552 S1 ;start wifi module ; Drives M569 P0 S1 ; Drive 0 goes forwards M569 P1 S1 ; Drive 1 goes forwards M569 P2 S0 ; Drive 2 goes forwards M569 P3 S1 ; Drive 3 goes forwards M569 P4 S0 ; Drive 4 goes forwards ;Independent motors leveling M584 X0 Y1 Z2:4 E3; two Z motors connected to driver outputs Z and E1 M671 X105:105 Y0:150 S1 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis M350 X16 Y16 Z16 E16 I1 ; Configure microstepping with interpolation M92 X80 Y80 Z80 E456 ; Set steps per mm M566 X900 Y900 Z1 E120 ; Set maximum instantaneous speed changes (mm/min) M203 X9000 Y9000 Z720 E1200 ; Set maximum speeds (mm/min) M201 X500 Y500 Z250 E250 ; Set accelerations (mm/s^2) M906 X1200 Y1200 Z2200 E1100 I0 ; Set motor currents (mA) and motor idle factor in per cent M84 S0 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; Set axis minima M208 X210 Y150 Z150 S0 ; Set axis maxima ; Endstops M574 X1 Y1 Z0 S0 ; Z-Probe ;M558 P1 I1 R0.4 F300 X0 Y0 Z0 M558 P8 H10 I1 R1 F600 X0 Y0 Z1 G31 X0 Y0 Z-0.25 P600 ; Heaters M140 H-1 ; Disable heated bed M305 P1 T100000 B4138 C0 R4700 ; Set thermistor + ADC parameters for heater 1 M143 H1 S280 ; Set temperature limit for heater 1 to 280C ; Fans M106 P0 H-1 ; set fan 1 to be gcode controlled M106 P2 S1 I0 T45 H1 ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned off ; Tools M563 P0 D0 H1 ; Define tool 0 G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C
Everything that I've pasted is indeed from the System tab under File Management in DWC.
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It really seems like your endstops are not actually working.
Can you confirm what firmware version is installed with M115?
And then can you confirm that the status of the endstops changes when you click them by checking with M119?
Earlier when you send M98 P"config.g" it didn't seem to echo anything back. Can you try again? There should be at least some response.
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The result of M115:
M115 FIRMWARE_NAME: RepRapFirmware for Duet 2 WiFi/Ethernet FIRMWARE_VERSION: 2.05.1 ELECTRONICS: Duet WiFi 1.02 or later FIRMWARE_DATE: 2020-02-09b
M119 correctly reports X and Y endstops (first/bottom is homed; then/middle is not; last/top is not for X and Y but I was tapping the nozzle to trigger the piezo):
M119 Endstops - X: not stopped, Y: not stopped, Z: not stopped, Z probe: at min stop M119 Endstops - X: not stopped, Y: not stopped, Z: not stopped, Z probe: not stopped M119 Endstops - X: at min stop, Y: at min stop, Z: not stopped, Z probe: not stopped
No echo on M98 P"config.g" only green background on the message.
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I guess your config.g is stripped down enough that some of the usual things like showing HTTP and FTP enabled etc aren't present, so there's nothing getting echoed.
Can you try adding M117 "Loading Config" to the end of config.g and when you save and reboot and send M98 P"config.g" again it should at least echo that.
Ok it looks like endstops are reporting correctly.
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;Home X and Y G91 ; relative positioning G1 Z5 F420 H2 ; Lower bed 5mm to ensure it is below the switch trigger height M400 M913 X50 Y50 ; set X Y motors to 50% of their normal current for homing G1 H1 X-375 Y-305 F600 ; course home X or Y G1 H1 X-375 F600 ; course home X G1 H1 Y-305 F600 ; course home Y G1 X5 Y5 F600 ; move away from the endstops G1 H1 X-10 F200 ; fine home X G1 H1 Y-10 F200 ; fine home Y G1 X5 Y5 F600 ; go to origin M400 M913 X100 Y100 ; set X Y motors to 100% of their normal current ;Home Z G90 ; absolute positioning G1 X30 Y30 F600 ; go to first probe point G30 ; home Z by probing the bed G91 ; relative positioning G1 Z5 F420 ; lift Z relative to current position G90 ; absolute positioning ;Load height map G29 S1
Does your homeall match that now after the corrections?
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When I run M98 P"config.g" I get no new messages in the console but I see a "Loading config" floating message in the bottom right part of DWC.
My homeall wasn't matching what you have laid out. The difference was the H1 instead of S1. In any case, there is no change - same behaviour and error. For the sake of completeness I ran that line by line as well and it again fails on G1 X5 Y5 F600 with Error: G0/G1: insufficient axes homed.
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
@fcwilt When I start with (G1 Z5 H2 F420) as per your suggestions I get a little but further, namely to G1 X5 Y5 F600 (line 8 in homeall.g) and I get the same error (Error: G0/G1: insufficient axes homed).
I don't understand what you mean by "get a little further"?
I just wanted you to execute that one command from the DWC console right after a reboot BEFORE doing anything else.
Frederick
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By a little bit further I mean that I manage to execute more lines compared than before i.e. a bit further down the list of lines. I might have misunderstood you then. The (G1 Z5 H2 F420) command executes fine and I'm able to get to G1 X5 Y5 F600 (line 8 in homeall.g) before I get the error.
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Ok at least we have confirmed that our config.g is being executed. You can delete the M117 now if you like.
At this point I think it may be useful to backup your current /sys folder files. (check box to highlight all files and then right click and download as zip.)
And then try a fresh config set from the web tool. something is wrong in there and it could even be hidden characters throwing it off. A fresh set of files would cross that off the list.
https://configtool.reprapfirmware.org/Start
If you have a recent config.json file in your /sys folder you can upload that to the tool to get your basic config settings populated, otherwise refer to the values from your existing config.g.
Bear in mind that you would need to manually add in the drive mapping for the second Z driver.
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I was actually going to bring up creating new config from scratch myself. I will do that (hopefully) tomorrow evening and report back.
Thanks all who tried to help!
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
By a little bit further I mean that I manage to execute more lines compared than before i.e. a bit further down the list of lines. I might have misunderstood you then. The (G1 Z5 H2 F420) command executes fine and I'm able to get to G1 X5 Y5 F600 (line 8 in homeall.g) before I get the error.
Thanks.
So the line G1 X5 Y5 F600 is the command that is generating the error?
Frederick
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
I'm able to get to G1 X5 Y5 F600 (line 8 in homeall.g) before I get the error.
Yes that line should back off the endstops fine because the endstops have already been triggered, which makes me think your endstops are inverted, but your trigger test with M119 seems to say the endstops are fine.
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I confirm that after setting up the firmware from scratch everything works as expected. There are still a couple of things that need to be ironed out but I think they go beyond the scope of this thread as tilt correction works.
Thanks to all who helped, I wish I could buy you each a beer!
Best
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
I confirm that after setting up the firmware from scratch everything works as expected. There are still a couple of things that need to be ironed out but I think they go beyond the scope of this thread as tilt correction works.
Thanks to all who helped, I wish I could buy you each a beer!
Best
Glad to hear its mostly sorted! Any chance you could post the relevant updated files for us to cruise through? Would be interesting to compare & learn from.
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@sebkritikel By all means! Bear in mind that I have made no changes of my own beyond what was discussed/posted in this thread (except for the fans but I find that irrelevant given the topic) - in other words, the new firmware is an amalgamation of the code cited here. In any case, I will link all relevant code snippets below in the hopes that they serve someone in the future.
bed.g
M561 ; clear any bed transform G28 ; home G30 P0 X105 Y0 Z-99999 ; probe near a leadscrew, half way along Y axis G30 P1 X105 Y150 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors
config.g
; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Printer Extrusions" ; set printer name M669 K1 ; select CoreXY mode ; Network M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet ; Drives M569 P0 S1 ; physical drive 0 goes forwards M569 P1 S1 ; physical drive 1 goes forwards M569 P2 S0 ; physical drive 2 goes backwards M569 P3 S1 ; physical drive 3 goes forwards M569 P4 S0 ; physical drive 4 goes backwards M584 X0 Y1 Z2:4 E3 ; set drive mapping M671 X105:105 Y0:150 S5 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z80 E456.00 ; set steps per mm M566 X900.00 Y900.00 Z1.00 E120.00 ; set maximum instantaneous speed changes (mm/min) M203 X6000.00 Y6000.00 Z1800.00 E1200.00 ; set maximum speeds (mm/min) M201 X500.00 Y500.00 Z250.00 E250.00 ; set accelerations (mm/s^2) M906 X1200 Y1200 Z1100 E1100 I30 ; set motor currents (mA) and motor idle factor in per cent M84 S30 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X210 Y150 Z150 S0 ; set axis maxima ; Endstops M574 X1 Y1 Z0 S0 ; Z-Probe M558 P8 H10 I1 R1 F600 X0 Y0 Z1 G31 X0 Y0 Z-0.25 P600 ; Heaters M140 H-1 ; disable heated bed M305 P1 T100000 B4138 R4700 ; set thermistor + ADC parameters for heater 1 M143 H1 S280 ; set temperature limit for heater 1 to 250C ; Fans M106 P0 S0 I0 F500 H-1 ; set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off M106 P1 S1 I0 F500 H1 T50 ; set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on ; Tools M563 P0 D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined ; Miscellaneous T0 ; select first tool
homeall.g
;Home X and Y G91 ; relative positioning G1 Z5 F420 H2 ; Lower bed 5mm to ensure it is below the switch trigger height M400 M913 X50 Y50 ; set X Y motors to 50% of their normal current for homing G1 H1 X-375 Y-305 F600 ; course home X or Y G1 H1 X-375 F600 ; course home X G1 H1 Y-305 F600 ; course home Y G1 X5 Y5 F600 ; move away from the endstops G1 H1 X-10 F200 ; fine home X G1 H1 Y-10 F200 ; fine home Y G1 X5 Y5 F600 ; go to origin M400 M913 X100 Y100 ; set X Y motors to 100% of their normal current ;Home Z G90 ; absolute positioning G1 X100 Y50 F600 ; go to first probe point G30 ; home Z by probing the bed G91 ; relative positioning G1 Z5 F420 ; lift Z relative to current position G90 ; absolute positioning ;Load height map G29 S1
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@equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:
@sebkritikel By all means! Bear in mind that I have made no changes of my own beyond what was discussed/posted in this thread (except for the fans but I find that irrelevant given the topic) - in other words, the new firmware is an amalgamation of the code cited here. In any case, I will link all relevant code snippets below in the hopes that they serve someone in the future.
config.g M671 X105:105 Y0:150 S5 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis
The only discernible change I see is the change from S1 to S5 - maybe thats all it took?
old M671 X105:105 Y0:150 S1 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis
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I tried changing from S5 to S1 and I observed no difference in the way the printer behaved.
As a side question, how do I mark the thread as Solved?