MFM recurring error
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@phaedrux As soon as the current job is complete I'll get some photos.
Assuming you want to see it mounted as well as on the bench and disassembled. -
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Have you tried re-printing the casing in higher quality?
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@phaedrux I havent but I can although the casing is clean on the inside. I had some first layer issues IIRC and it still has some dry bedweld on it (got distracted and forgot to rinse).
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@infiniteloop I have the MFM sitting directly atop the extruder and the PTFE tube comes in close to vertical so I'm not concerned about the angle of the filament path.
I am considering picking up a piece of copper tube from McMaster and replacing the bit of PTFE tubing connecting the MFM to the extruder but I really dont think that's where the problem is.
I'm inclined to print a new casing and giving that a try as I noticed that the ring on the MFM sensor from the magnet rubbing was a partial circle which would indicate to me that there's a slight tilt to the magnet.
I think an injection molded case would remove any uncertainty around it but I'm not certain that would resolve this issue.
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@wouldstain said in MFM recurring error:
I think an injection molded case would remove any uncertainty around it but I'm not certain that would resolve this issue.
My MFM works reliably, the electronics are pretty well engineered. The - self-printed - case needed heavy postprocessing, I had to file, drill, cut and sand a lot. Especially the filament path and the idler are problematic, the often mentioned distance between magnet and sensor is no theme anymore since introduction of the 2 mm magnet in v2. So yes, an injection molded case would be helpful.
Given the high precision of detected filament movement, a direct coupling with the extruder - or better, an integrated design - is still on my wish list …
But, again: if the magnet rotates as intended, PCB and I2C transmission work flawlessly. @dc42 has made a remarkable job to ensure reliability of the data, so, as long as we get our cables right, we won't run into problems on this side. Simply put: it's the mechanics we have to take care of.
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@infiniteloop No doubt! I'm still pretty new at this and I generally assume it's something I'm doing. Given what you're saying about post processing and my questionable print quality, I would not be surprised if there are tolerance issues with my casing.
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@phaedrux
Finally got around to reprinting case. Used PLA this time instead of PETG.
It's alot cleaner on the outside but really no difference on the inside.
I ran a needle file through the feed path just to be certain there's no blobs or burrsInitial reading (before printing first time). As you can see, AGC has gone up quite a bit.
Duet3D rotating magnet filament monitor v3 on pin e0stop, enabled, sensitivity 28.80mm/rev, allow 60% to 160%, check printing moves every 3.0mm, version 3, mag 133 agc 111, no calibration data
1st test / calibration print on 20mm calibration cube:
35% ona "too little movement error":
Duet3D rotating magnet filament monitor v3 on pin e0stop, enabled, sensitivity 28.80mm/rev, allow 60% to 160%, check printing moves every 3.0mm, version 3, mag 132 agc 109, measured sensitivity 25.84mm/rev, min 35% max 106% over 983.4mm
adjusted M591 while paused to:
M591 P3 C"e0_stop" S1 D0 L25.84 R35:130Print completed without further error.
2nd test completed without error.
3rd test printed 2 x 20mm calibration cubes simultaneously
Stopped at 88% with the following:
M591 d0
Duet3D rotating magnet filament monitor v3 on pin e0stop, enabled, sensitivity 25.84mm/rev, allow 35% to 130%, check printing moves every 3.0mm, version 3, mag 132 agc 109, measured sensitivity 26.05mm/rev, min 0% max 109% over 2811.8mmSo... Even with the new case, it's still randomly stopping.
I'm thinking there's a problem with the MFM.
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Please send an email to warranty@duet3d.com and CC your reseller. Include a link to this forum thread and the details of your original purchase. You'll receive a reply with a form to fill out.
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@phaedrux done. thank you!