Solved 3.2 SBC cancel print not working w/ missing/blank cancel.g
-
Hi there. I have a problem.
If I have to cancel a print and start this or another, the extruder no longer feeds filament.
Only when I reboot the Raspberry Pi 4 does the pressure go back to normal.
Use a Duet3 6hc with Raspberry Pi 4.
It can be reproduced at any time. -
Can you post your config.g file along with the pause.g and cancel.g if you have one.
Can you also confirm the firmware version you are currently running? -
; Configuration file for Duet 3 (firmware version 3) ; executed by the firmware on start-up ; ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit) ; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Duet3" ; set printer name M912 P0 S-5 ; sstzt CPU Temp korrektur M669 K1 ;switch to core X/Y mode ; Drives M569 P0.0 S0 D3 V50 H50 ; X physical drive 0.0 goes forwards M569 P0.1 S0 D3 V50 H50 ; Y physical drive 0.1 goes forwards M569 P0.2 S1 D3 V50 H50 ; Z1 physical drive 0.2 goes forwards M569 P0.3 S1 D3 V50 H50 ; Z2 physical drive 0.3 goes forwards M569 P0.4 S1 D3 V50 H50 ; Z3 physical drive 0.4 goes forwards M569 P0.5 S0 D3 ; E physical drive 0.5 goes backwards ; Stealthchop M915 P0.0 T50 M915 P0.1 T50 M915 P0.2 T50 M915 P0.3 T50 M915 P0.4 T50 M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5 ; set drive mapping M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z800.00 E462.10 ; set steps per mm M566 X850.00 Y850.00 Z200.00 E800.00 ; set maximum instantaneous speed changes (mm/min) M203 X8000.00 Y8000.00 Z500.00 E5000.00 ; set maximum speeds (mm/min) M201 X900.00 Y900.00 Z100.00 E800.00 ; set accelerations (mm/s^2) M906 X1075 Y1075 Z1000 E950 I50 ; set motor currents (mA) and motor idle factor in per cent M84 S120 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X300 Y300 Z295 S0 ; set axis maxima ; Endstops M574 X1 S1 P"io2.in" ; configure active-high endstop for low end on X via pin io2.in M574 Y1 S1 P"io1.in" ; configure active-high endstop for low end on Y via pin io1.in M574 Z1 S2 ; Z-Probe M950 S0 C"io7.out" ; create servo pin 0 for BLTouch M558 P9 C"^io7.in" H5 F300 T3000 ; set Z probe type to bltouch and the dive height + speeds G31 P500 X38.884 Y2.578 Z0.00 ; set Z probe trigger value, offset and trigger height M557 X40:260 Y40:260 S40 ; define mesh grid M671 X-33.985:142.224:318.433 Y-16.206:312.004:-16.206 S50 ; Z lift Point Position ; Heaters M308 S0 A"Bett" P"temp0" Y"thermistor" T100000 B4100 ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0 M307 H0 A176.1 C1192.2 D31.2 S1.0 V24.3 B0 ; disable bang-bang mode for the bed heater and set PWM limit M140 H0 ; qmap heated bed to heater 0 M143 H0 S140 ; set temperature limit for heater 0 to 120C M308 S1 A"Vulcano" P"temp1" Y"thermistor" T100000 B4610 C7.060000e-8 ; configure sensor 1 as thermistor on pin temp1 M950 H1 C"out2" T1 ; create nozzle heater output on out1 and map it to sensor 1 M307 H1 A367.3 C225.2 D2.8 S0.5 V24.6 B0 ; disable bang-bang mode for heater and set PWM limit M308 S2 A"Elektro" P"temp3" Y"thermistor" T100000 B4100 ; configure sensor 1 as thermistor on pin temp1 M308 S3 Y"drivers" A"Stepper" ; configure sensor 3 as temperature warning and overheat flags on the TMC2660 on Duet M308 S4 Y"mcu-temp" A"MCU" ; configure sensor 4 as thermistor on pin e1temp ; Fans M950 F1 C"out7" Q500 ; create fan 1 on pin out7 and set its frequency M106 P1 C"Hotend" S1 H1 T50 ; set fan 1 name and value. Thermostatic control is turned on M950 F0 C"out4" Q2500 ; create fan 0 on pin out4 and set its frequency M106 P0 C"Bauteil1" S0 H-1 ; set fan 0 name and value. Thermostatic control is turned off M950 F2 C"out9" Q500 ; create Light on pin out9 and set its frequency M106 P2 C"Licht" S0 H-1 M950 F3 C"out8" Q500 ; create fan 3 on pin out8 and set its frequency M106 P3 H3:4 T38 ; set fan 3 value ; Tools M563 P0 S"Vulcano" D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined M564 S1 H0 T0 ; Miscellaneous ;M575 P1 S1 B57600 ; enable PanelDue M911 S21 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss M501 ; load saved parameters from non-volatile memory
; pause.g ; called when a print from SD card is paused ; ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:59 GMT+0200 (Mitteleuropäische Sommerzeit) M83 ; relative extruder moves G1 E-10 F3600 ; retract 10mm of filament G91 ; relative positioning G1 Z5 F360 ; lift Z by 5mm G90 ; absolute positioning G1 X0 Y0 F6000 ; go to X=0 Y=0
EndGcode when print is finish M104 S0 M140 S0 ;Retract the filament G92 E1 G1 E-5 F200 G1 X5 Y300 F6000 G1 Z290 F500 M300 S290 P1000 M84 M98 P"/macros/LED/LED_gruen" G4 S30 M98 P"/macros/LED/LED_weiss" G4 S120 M98 P"/macros/LED/LED_aus"
I doun't have a cancel.g.
I use RRF 3.2 stabel.
-
is there an error message in the console?
-
No there is no error on console
-
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode) Board ID: 08DJM-956L2-G43S8-6JTDG-3SJ6P-KB0UG Used output buffers: 1 of 40 (10 max) === RTOS === Static ram: 149788 Dynamic ram: 63788 of which 64 recycled Never used RAM 145192, free system stack 124 words Tasks: Linux(ready,71) HEAT(blocked,296) CanReceiv(blocked,927) CanSender(blocked,346) CanClock(blocked,352) TMC(blocked,19) MAIN(running,717) IDLE(ready,19) Owned mutexes: HTTP(MAIN) === Platform === Last reset 02:30:34 ago, cause: software Last software reset at 2021-01-13 09:03, reason: User, none spinning, available RAM 145192, slot 1 Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 Aux1 errors 0,0,0 MCU temperature: min 34.4, current 35.1, max 42.7 Supply voltage: min 24.3, current 24.7, max 25.3, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0 Driver 0: position 0, standstill, reads 17103, writes 43 timeouts 0, SG min/max 0/0 Driver 1: position 0, standstill, reads 17103, writes 43 timeouts 0, SG min/max 0/0 Driver 2: position 85642, standstill, reads 17091, writes 55 timeouts 0, SG min/max 0/0 Driver 3: position 0, standstill, reads 17091, writes 55 timeouts 0, SG min/max 0/0 Driver 4: position 0, standstill, reads 17092, writes 55 timeouts 0, SG min/max 0/0 Driver 5: position 0, standstill, reads 17103, writes 44 timeouts 0, SG min/max 0/1023 Date/time: 2021-01-13 11:34:33 Slowest loop: 180.92ms; fastest: 0.04ms === Storage === Free file entries: 10 SD card 0 not detected, interface speed: 37.5MBytes/sec SD card longest read time 0.0ms, write time 0.0ms, max retries 0 === Move === DMs created 125, maxWait 1171149ms, bed compensation in use: mesh, comp offset 0.000 === MainDDARing === Scheduled moves 19083, completed moves 19083, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 11], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 === GCodes === Segments left: 0 Movement lock held by null HTTP* is doing "M122" in state(s) 0 Telnet is idle in state(s) 0 File* is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger* is idle in state(s) 0 Queue* is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 36177, send timeouts 81349, received 0, lost 0, longest wait 0ms for reply type 0, free buffers 48 === SBC interface === State: 4, failed transfers: 0 Last transfer: 2ms ago RX/TX seq numbers: 44017/44017 SPI underruns 0, overruns 0 Number of disconnects: 2, IAP RAM available 0x2c8a8 Buffer RX/TX: 0/0-0 === Duet Control Server === Duet Control Server v3.2.0 Code buffer space: 4096 Configured SPI speed: 8000000 Hz Full transfers per second: 38.93 Maximum length of RX/TX data transfers: 2672/1504
-
@Heartleander81 said in Problem after cancel print:
I doun't have a Cancel.g to time.
What does that mean?
Is the code you posted in cancel.g?
In the code posted you are setting the temps to zero. When you try to print again do you restore the correct settings?
Frederick
-
The last config is my end GCode afte the print.
-
In the code posted you are setting the temps to zero. When you try to print again do you restore the correct settings?
Frederick
I doun't know. I start the gcode. The bed heats up, the nozzle heats up, then make the printer his homing. Then extrude any filament. After this doun't come filament out the nozzel.
-
There is a picture oft the DWC .
Print is at layer 71 and filament only used 0.4mm, but must ~100mm used at this layer hight.I hope you understand what i mean. My english is not the best
-
Hi,
This is a long shot but create an empty cancel.g file and see if that makes a difference.
Frederick
-
@fcwilt Will test it after work. But just think that I have an error somewhere in a file. After successfully printing the file, the problem was that the next print did not work either. It only worked again after restarting the Pi. That's only since I updated from 3.1.1 to 3.2.0
-
@Heartleander81 said in Problem after cancel print:
If I have to cancel a print and start this or another, the extruder no longer feeds filament.
Only when I reboot the Raspberry Pi 4 does the pressure go back to normal.Can you try describing again what exactly this means? I'm having a hard time understanding the problem.
Does the printer try to resume the print but the extruder motor doesn't turn?
Does it just sit there?
Is the heater at temp at that point?
-
@Phaedrux
I start a print.
For example, a component comes loose.
Then press pause and release the pressure.
Change something on the slice or try to reprint.
Then nothing is extruded during printing.
When I restart the Pi, it prints normally.
But today I was able to determine that this problem also occurred even after a successful print. That's only since the update from 3.1.1 to 3.2.0After Bed and Nozzle is on temp make my Printer Homing.
-
-
Sorry. Fu.. Translator. I doun't have check before copy and past.PRESS pause and then cancel i the print
I have a Video on youtube
-
Did you try creating the missing cancel.g?
-
This post is deleted! -
Is the same with empty cancel.g
-
Do you have a
T0
command in your slicer start gcode?
Is your tool still selected after canceling?
Can you try putting some commands in your cancel.g?Example:
; cancel.g ; ; Run when the print is paused, and then canceled. ; G10 P0 R0 S0 ; Set hotend temp to 0 M140 S0 ; Set bed temp to 0 M106 S255 ; Fan at 100 to cool nozzle and bed M220 S100 ; Set speed factor back to 100% in case it was changed M221 S100 ; Set extrusion factor back to 100% in case it was changed M290 R0 S0 ; clear babystepping G28 XY ; home XY M84 ; turn off steppers G4 S60 ; wait 1 minute for nozzle to cool M107 ; turn off the fan