Wrong position after homing axes
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@coolm8 said in Wrong position after homing axes:
duet IR/Probe
there is no way that you are using this probe and not having an offset.
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I did add the offset in X of 40 so now i have:
M558 P1
G31 P500 X40 Y0 Z0.35But still no difference.
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execute your homeall manually (entering each statement in the console). which one of the commands is producing the noise.
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Ok, did not think about that.
It is the following command. G30
Strange thing is that if I remove that from homeall.g, it does not probe the bed, but it still has this strange movement in Y and then goes to wrong home position.So homeall.g looks like this now and i can execute every step manualyl without issue:
; Relative positioning
G91; Lift Z
G1 Z5 F6000; Course home X and Y
G1 X-210 Y-210 F1800 S1; Move away from the endstops
G1 X5 Y5 F6000; Fine home X and Y
G1 X-210 Y-210 F360 S1; Absolute positioning
G90; Go to first bed probe point and home Z
G1 X0 Y15 F1800 -
G30 determines z=0 by moving the bed up until it triggers the probe.
maybe the bed is touching the hotend before the probe triggers. that could make some noise.does the strange movement happen when you execute G1 X0 Y15 F1800 ?
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No, the bed is not touching the sensor. homez.g does also contain the command G30. If i removed from there i get the error 'homing Z failed'.
After all axes are hommed i can execute G30 without any issue.So for me it seems like this is the issue:
homing X and Y puts the printhead at front left corner of the printer, stopped by endstops at Xmin and Ymin. Then i can move the printhead just fine with manual commands.
As soon as G30 gets executed the firmware thinks the print area is about X40 Y0, so the initial movement of G30 from X0 Y0 to X0 Y15 makes this strange motor noise. After it has done the probing an the printhead moves to X40 Y0 and resets the coordinates to X0 Y0. From then on G30 does exactly the same movements as before without any strange noise and smoothly running motors.Somehow I believe the printer thinks moving from real X0 Y0 to X0 Y15 is an impossible move (the motors sound quit like when the run in to force and cannot move any further), but it still executes it.
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hmm your config seems to be missing the
M574 Z1 S2 ; set endstops controlled by probe -
@coolm8 said in Wrong position after homing axes:
Somehow I believe the printer thinks moving from real X0 Y0 to X0 Y15 is an impossible move (the motors sound quit like when the run in to force and cannot move any further), but it still executes it.
find out where its grinding on. the endstops?
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It is not grinding anywhere. It makes the move correctly just the sound is weird.
This is not a mechanical issue, it is only software side.
It only happens wile probing, i can make exactly the same move just fine before the Z-axis is homed (i cannot do it afterwards because the software does not allow me to go negativ on the X axis).I alread had the following:
M574 X1 Y1 Z1 S0changing to the following did not bring any changes:
M574 X1 Y1 S0
M574 Z1 S2Why is G30 affecting the X and Y axes anyway?
Might it be that i have the Duet Wifi 1 but running recently updated Version:
Firmware Electronics: Duet WiFi 1.0 or 1.01
Firmware Version: 2.03 (2019-06-13b2)
WiFi Server Version: 1.23
Web Interface Version: 1.22.6 -
@coolm8 said in Wrong position after homing axes:
M558
its not but it might be picking up your X1 in M558 command
try replacing the entire line with
M558 P1 H5 F120 T6000 ; set Z probe type to unmodulated and the dive height + speeds -
@veti said in Wrong position after homing axes:
M558 P1 H5 F120 T6000
This still has no effect on this behavior.
To be exact, the X offset after homing is 58mm. When execute an emergency stop after homing Z, I can move the X-axis to -58 until the endstop triggers. I then can manually go forward 204mm until I reach the end of the other side of the X axis (from -58 to 164). This shows that the motors and the stepping is set up correctly.I have taken a video of the steps from Z-Axis homing. The strange movement beginns at 1:00 minute into the video. See: https://youtu.be/9m7Y-PwS-pI
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the video is private
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@coolm8 said in Wrong position after homing axes:
M564 H0
can you remove this? this should not be in a normal config.
also the normal place for the M208 command is after the M84. This should not be a problem for your config i think, but on certain commands the order is important.
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If I remove M554 H0 I cannot home any axis anymore. No matter what i choose homeall, home X, ... I get this error: G0/G1: insufficient axes homed
I fixed the video and it should now be accessible:
https://youtu.be/9m7Y-PwS-pI -
@coolm8 said in Wrong position after homing axes:
If I remove M554 H0 I cannot home any axis anymore. No matter what i choose homeall, home X, ... I get this error: G0/G1: insufficient axes homed
This is because of this
@coolm8 said in Wrong position after homing axes:
; Lift Z
G1 Z5 F6000You need to add S2 to that G1 Z move so that it can move without being homed first.
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This is not what I'm looking for. I do not need to disable manual movement before homing and i do not need to overwrite that with manual commnands to move. All i want is G30 to work properly and not do to that strange additional movement that you can see in the video.
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Can you send
G31 P1
in the gcode console? I suspect that the offset may not be applied correctly.Have you verified that the steps per mm is correct so that 10mm of requested movement equals 10mm of actual movement?
@coolm8 said in Wrong position after homing axes:
This is not what I'm looking for. I do not need to disable manual movement before homing and i do not need to overwrite that with manual commnands to move.
You can do as you wish, I'm merely explaining what's happening. Please keep in mind that we are only trying to volunteer our time to help you solve your problem. If you would prefer, I can stop trying to assist.
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I did not want to be rude. I just wanted to clarify what I'am trying to solve. Any help is welcome and I am thankful for all your support. Too sad it has not helped yet.
G31 P1 does not do anything. Do I understand correctly that it should set the probe trigger value? Should the change be visible in the web view?
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In the gcode console, what does M558 return?
Try sending
M558 P1 H5 F120 T6000
G31 P500 X40 Y0 Z0.35
Then alter your homeall "first probe point" to move the probe to the center of the bed. Say G1 X100 Y100. Before the G30.
and then test homing all.
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@phaedrux said in Wrong position after homing axes:
G31 P500 X40 Y0 Z0.35
Hmm, this is strange. Now it behaves completely different. The final position after G30 is now at X100 Y100 but the probed point which should be X100 Y100 is done at X0 Y100.
As long is I do not execute G30 the axes are working correctly. Homing X and Y puts the head to left front corner, G1 X100 Y100 moves the head to the center. According to the documentation I have set the front left corner to be 0,0. Somehow after G30, X100 Y100 is 0,0.