RepRapFirmware 3.6.0-alpha.4+3 available for testing
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@balajiramani I run delta calibration using the smart effector probe without any obvious problem, with residual error usually under 0.02. I normally don't need to use mesh compensation.
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Just the the update earlier this evening and started a test print, and now I'm experiencing the same step timing issue as mentioned above.
D3 Mini with 1LC in standalone mode.
There printer is currently halted with this error message:
30.8.2024, 18:29:54 Error: Movement halted because a step timing error occurred (code 3). Please reset the controller. 30.8.2024, 17:55:27 ABS filament loaded ABS filament loaded & config applied 30.8.2024, 17:54:49 16 points probed, min error -0.030, max error 0.016, mean -0.012, deviation 0.013 Height map saved to file 0:/sys/heightmap.csv Height map saved to file 0:/sys/adaptive_heightmap.csv 30.8.2024, 17:54:18 Default grid: X10.0:340.0, Y10.0:340.0, Number of points: X12 Y12, 144 points Adaptive grid: X120.833:229.167, Y120.833:229.136, Number of points: X4 Y4, 16 points 30.8.2024, 17:53:57 M32 "0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode" File 0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode selected for printing
This is the M122 outputs:
30.8.2024, 20:23:58 M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ Used output buffers: 11 of 40 (37 max) === RTOS === Static ram: 92328 Dynamic ram: 95720 of which 0 recycled Never used RAM 45628, free system stack 126 words Tasks: NETWORK(1,ready,19.3%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.0%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,794) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,339) MAIN(1,running,77.6%,627) IDLE(0,ready,1.4%,29) AIN(4,delaying,0.8%,259), total 100.0% Owned mutexes: === Platform === Last reset 02:41:46 ago, cause: software Last software reset at 2024-08-30 17:42, reason: User, Gcodes spinning, available RAM 52612, slot 0 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 MCU temperature: min 45.7, current 46.0, max 46.0 Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/916/440, gc cycles 2170 Events: 0 queued, 0 completed Date/time: 2024-08-30 20:23:53 Slowest loop: 46.99ms; fastest: 0.13ms === Storage === Free file entries: 17 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 5.7ms, write time 7.2ms, max retries 0 === Move === Segments created 178, maxWait 0ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/39.68ms), max steps late 0, ebfmin 0.00, ebfmax 0.00 Pos req/act/dcf: -3086.00/-3086/0.45 -23971.00/-23971/0.43 33160.00/33160/-0.00 no step interrupt scheduled Driver 0: standstill, SG min 8, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 2, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 2, read errors 0, write errors 0, ifcnt 23, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 5: not present Driver 6: not present === DDARing 0 === Scheduled moves 66586, completed 66560, LaErrors 0, Underruns [0, 0, 0] === DDARing 1 === Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0] === Heat === Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.4 Heater 1 is on, I-accum = 0.0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is doing "G1 X192.529 Y130.297 E.90485" in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P250" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 1, axes/extruders owned 0x0000807 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 0 clear 0 Extruder 0 sensor: no filament === CAN === Messages queued 247, received 600, lost 0, ignored 0, errs 0, boc 0 Longest wait 6ms for reply type 6024, peak Tx sync delay 132, free buffers 26 (min 25), ts 128/128/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 20.21ms; fastest: 0.07ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 1 of 8 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1.0 MAC address c4:5b:be:ce:91:93 Module reset reason: Power up, Vcc 3.37, flash size 2097152, free heap 43044 WiFi IP address 192.168.30.50 Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0 30.8.2024, 20:23:54 M122 B121 Diagnostics for board 121: Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4+3 (2024-08-28 11:24:12) Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25) All averaging filters OK Never used RAM 6672, free system stack 79 words Tasks: Move(3,nWait 7,0.0%,84) TMC(2,delaying,3.6%,52) HEAT(2,nWait 6,0.4%,88) CanAsync(5,nWait 4,0.0%,48) CanRecv(3,nWait 1,0.0%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,91.0%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0% Owned mutexes: Last reset 02:41:43 ago, cause: power up Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0 Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0 Moves scheduled 65223, hiccups 0 (39.68/39.68ms), segs 58, step errors 0 (types 0x0), maxLate 0 maxPrep 0, ebfmin 0.00 max 0.00 Peak sync jitter -1/8, peak Rx sync delay 199, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3459548387 ticks, disabled VIN voltage: min 24.5, current 24.5, max 24.6 MCU temperature: min 41.1C, current 75.3C, max 75.5C Driver 0: pos 2824553, 568.8 steps/mm, standstill, SG min 2, read errors 0, write errors 0, ifcnt 12, reads 9061, writes 0, timeouts 0, DMA errors 0, CC errors 0 Last sensors broadcast 0x00000012 found 2 164 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 405, send timeouts 0, received 171, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 18, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0 Accelerometer: LIS3DH, status: 00 I2C bus errors 0, naks 0, contentions 0, other errors 0 === Filament sensors === Interrupt 5726621 to 0us, poll 9 to 925us Driver 0: ok
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Thanks everyone, looks like we are getting a lot more step error code 3 than before with this build.
We've found a few other issues too:
- After a homing move there was sometimes a short pause before movement resumes. This is now fixed in the 3.6-dev source code. It may affect probing moves too.
- When an endstop switch is triggered during a homing move and the drivers concerned are on an expansion board, it's normal for the expansion board motor(s) to overshoot very slightly and then move back to the correct position. However, in this release the overshoot is often somewhat greater than it is in RRF 3.5.3-rc1, resulting in a noticeable jolt. This occurs with main board firmware 3.6.0-alpha.4+3 even if the expansion board is running firmware 3.5.3-rc.1.
- When EXP1HCL boards running 3.6.0-alpha.4+3 firmware are used in open loop mode, the start and end of the moves are jerky. Closed loop and assisted open loop modes work properly. This probably affects M23CL motors too.
I won't be able to fix these issues for a while because of other commitments.
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Folks if anyone has a print that generates a "Movement halted error" after a short time (so relatively early in the print) can you please post the gcode file and the config.g file for the printer. That way we can try and reproduce the issue.
@Exerqtor did your error occur on the first print after a printer restart or had you already printed a previous file? I ask because your m122 is showing a hiccup delay, but no hiccups (maybe you have run m122 more than once after the failure). If this was the second print that failed can you test to see if the same print fails as the first print after the printer is restarted?
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@Adrian52 I haven't been able to run a successful delta calibration with the 3.6.0 firmware. This was not an issue in 3.5.2. The head crashes into the bed. The movement is not straight from one probe point to the other and it more of a 'U' shaped move. Can you post your bed.g, so that I can compare it with what I have?
Thanks,
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@balajiramani a U shaped move suggests that the auto-generated travel move is not being segmented. Please run M669 without parameters, to check that segmentation hasn't been disabled. Also please send M115 to verify that you really are running the latest alpha firmware.
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@dc42 Here are the output of the commands:
8/31/2024, 1:20:52 PM M115 FIRMWARE_NAME: RepRapFirmware for Duet 2 WiFi/Ethernet FIRMWARE_VERSION: 3.6.0-alpha.4+3 ELECTRONICS: Duet WiFi 1.0 or 1.01 FIRMWARE_DATE: 2024-08-28 10:03:28 8/31/2024, 1:20:40 PM M669 Kinematics is Linear delta, 100 segments/sec, min. segment length 0.20mm
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Those of you with the code 3 errors, how long was the print running? I think I've just found a bug that could cause a code 3 error if a print was running about 47 minutes after the Duet 3 was booted up (about 38 minutes for Duet 2).
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@balajiramani thanks. Are you sure that the delta radius and rod length are set to approximately the correct value before calibration? I don't think anyone else has reported issues with delta calibration running recent 3.6.0 alpha versions, and calibration works perfectly on my own delta. So I am wondering whether the reason for the U-shaped moves is that either the rod length or delta radius is set incorrectly. Possibly there is an error in your M665 or M666 command and RRF 3.6 responds differently to that error. So please run M665 and M666 without parameters and check that the reported values are as expected.
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@dc42 Duet 2 Wifi on an Ender 5 plus stopped with the code 3 error. Your 38 minute mark sounds about right but I don't have an exact time when it stopped.
I installed 3.5.3 rc1 and ran the same gcode without issues.
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@gloomyandy said in RepRapFirmware 3.6.0-alpha.4+3 available for testing:
Folks if anyone has a print that generates a "Movement halted error" after a short time (so relatively early in the print) can you please post the gcode file and the config.g file for the printer. That way we can try and reproduce the issue.
For me it happened roughly 35min into the print.
@Exerqtor did your error occur on the first print after a printer restart or had you already printed a previous file? I ask because your m122 is showing a hiccup delay, but no hiccups (maybe you have run m122 more than once after the failure). If this was the second print that failed can you test to see if the same print fails as the first print after the printer is restarted?
Yeah it was the first print after the update! And you're right, it was the second M122 output. Here is the first output (including the print startinfo, error message etc:
30.8.2024, 20:23:36 M122 B121 Diagnostics for board 121: Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4+3 (2024-08-28 11:24:12) Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25) All averaging filters OK Never used RAM 6672, free system stack 79 words Tasks: Move(3,nWait 7,0.3%,84) TMC(2,nWait 6,3.6%,52) HEAT(2,nWait 6,0.4%,88) CanAsync(5,nWait 4,0.0%,48) CanRecv(3,nWait 1,0.1%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,90.5%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0% Owned mutexes: Last reset 02:41:25 ago, cause: power up Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0 Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0 Moves scheduled 65223, hiccups 782 (39.68/39.68ms), segs 58, step errors 2 (types 0x8), maxLate 0 maxPrep 1303, ebfmin 0.00 max 0.00 Peak sync jitter -4/10, peak Rx sync delay 255, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3473139117 ticks, disabled VIN voltage: min 23.7, current 24.5, max 25.0 MCU temperature: min 41.1C, current 75.4C, max 75.5C Driver 0: pos 2824553, 568.8 steps/mm, standstill, SG min 0, read errors 1, write errors 0, ifcnt 12, reads 44905, writes 12, timeouts 3, DMA errors 0, CC errors 0, failedOp 0x6f Last sensors broadcast 0x00000012 found 2 43 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 200813, send timeouts 0, received 154587, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 17, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 825, adv 35393/74627 Accelerometer: LIS3DH, status: 00 I2C bus errors 0, naks 3, contentions 0, other errors 0 === Filament sensors === Interrupt 5726621 to 0us, poll 4 to 2225us Driver 0: ok 30.8.2024, 20:23:32 M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ Used output buffers: 4 of 40 (37 max) === RTOS === Static ram: 92328 Dynamic ram: 95720 of which 0 recycled Never used RAM 45628, free system stack 126 words Tasks: NETWORK(1,ready,18.9%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.3%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,794) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,339) MAIN(1,running,77.7%,627) IDLE(0,ready,1.2%,29) AIN(4,delaying,0.8%,259), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 02:41:20 ago, cause: software Last software reset at 2024-08-30 17:42, reason: User, Gcodes spinning, available RAM 52612, slot 0 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,1,0 MCU temperature: min 35.7, current 46.0, max 46.6 Supply voltage: min 2.7, current 23.9, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/1396/920, gc cycles 2164 Events: 0 queued, 0 completed Date/time: 2024-08-30 20:23:27 Slowest loop: 223.44ms; fastest: 0.10ms === Storage === Free file entries: 17 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 10.2ms, write time 69.6ms, max retries 0 === Move === Segments created 178, maxWait 603453ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/39.68ms), max steps late 0, ebfmin 0.00, ebfmax 0.00 Pos req/act/dcf: -2663.00/-3086/0.45 -23548.00/-23971/0.43 33160.00/33160/-0.00 no step interrupt scheduled Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 50443, writes 47, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 50443, writes 47, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 50467, writes 22, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 50467, writes 22, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 23, reads 50467, writes 23, timeouts 0, DMA errors 0, CC errors 0 Driver 5: not present Driver 6: not present === DDARing 0 === Scheduled moves 66586, completed 66560, LaErrors 217, Underruns [0, 0, 0] === DDARing 1 === Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0] === Heat === Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.4 Heater 1 is on, I-accum = 0.0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is doing "G1 X192.529 Y130.297 E.90485" in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P250" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 1, axes/extruders owned 0x0000807 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 0 clear 0 Extruder 0 sensor: no filament === CAN === Messages queued 154539, received 200688, lost 0, ignored 0, errs 1318, boc 0 Longest wait 7ms for reply type 6029, peak Tx sync delay 10782, free buffers 26 (min 24), ts 48405/48403/0 Tx timeouts 0,0,1,0,0,0 last cancelled message type 30 dest 127 === Network === Slowest loop: 210.77ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 1 of 8 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1.0 MAC address c4:5b:be:ce:91:93 Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 43020 WiFi IP address 192.168.30.50 Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0 30.8.2024, 18:29:54 Error: Movement halted because a step timing error occurred (code 3). Please reset the controller. 30.8.2024, 17:55:27 ABS filament loaded ABS filament loaded & config applied 30.8.2024, 17:54:49 16 points probed, min error -0.030, max error 0.016, mean -0.012, deviation 0.013 Height map saved to file 0:/sys/heightmap.csv Height map saved to file 0:/sys/adaptive_heightmap.csv 30.8.2024, 17:54:18 Default grid: X10.0:340.0, Y10.0:340.0, Number of points: X12 Y12, 144 points Adaptive grid: X120.833:229.167, Y120.833:229.136, Number of points: X4 Y4, 16 points 30.8.2024, 17:53:57 M32 "0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode" File 0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode selected for printing
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@dc42 Awesome, i will install it and try the same testprint right away
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@dc42 The delta calibration procedure works fine with 3.5.2. With 3.6.0-alpha*, I run into the issue. I checked the values of M665 and M666 in both 3.5.2 and 3.6.0-alpha and they are the same values.
Here is what I see with 3.5.2:
8/31/2024, 5:09:41 PM M666 Endstop adjustments X-1.26 Y-1.03 Z2.30, tilt X0.00% Y0.00% 8/31/2024, 5:09:38 PM M665 Diagonals 395.647:395.647:395.647, delta radius 214.803, homed height 359.884, bed radius 160.0, X -0.068°, Y -0.015°, Z 0.000°
Here is what I see with 3.6.0-alpha.4+3
8/31/2024, 5:58:57 PM M666 Endstop adjustments X-1.26 Y-1.03 Z2.30, tilt X0.00% Y0.00% 8/31/2024, 5:58:56 PM M665 Diagonals 395.647:395.647:395.647, delta radius 214.803, homed height 359.884, bed radius 160.0, X -0.068°, Y -0.015°, Z 0.000°
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@balajiramani Hi - sorry for the delay
here is my bed.g. I have a 250mm dia round bed; Auto calibration routine for large delta printer M561 ; clear any bed transform ; If the printer hasn't been homed, home it ;if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed G28 ; Probe the bed and do auto calibration G1 X-70 Y-60 Z10 F6000 ; go to just above the first probe point while true if iterations = 5 abort "too many auto calibration attempts" G30 P0 X-70 Y-60 Z-99999 if result != 0 continue G30 P1 X-85 Y0 Z-99999 if result != 0 continue G30 P2 X-50 Y75 Z-99999 if result != 0 continue G30 P3 X0 Y85 Z-99999 if result != 0 continue G30 P4 X50 Y75 Z-99999 if result != 0 continue G30 P5 X85 Y0 Z-99999 if result != 0 continue G30 P6 X75 Y-50 Z-99999 if result != 0 continue G30 P7 X0 Y-85 Z-99999 if result != 0 continue G30 P8 X-40 Y-40 Z-99999 if result != 0 continue G30 P9 X-50 Y0 Z-99999 if result != 0 continue G30 P10 X-40 Y40 Z-99999 if result != 0 continue G30 P11 X0 Y50 Z-99999 if result != 0 continue G30 P12 X40 Y40.00 Z-99999 if result != 0 continue G30 P13 X50 Y0 Z-99999 if result != 0 continue G30 P14 X40 Y-40 Z-99999 if result != 0 continue G30 P15 X-4 Y-2 Z-99999 if result != 0 continue G30 P16 X4 Y-2 Z-99999 if result != 0 continue G30 P17 X0 Y4 Z-99999 S6 if result != 0 continue if move.calibration.final.deviation <= 0.03 break echo "Repeating calibration because deviation is too high (" ^ move.calibration.final.deviation ^ "mm)" ; end loop echo "Auto calibration successful, deviation", move.calibration.final.deviation ^ "mm" G1 X0 Y0 Z150 F5000 ; get the head out of the way M500 G28
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I've put the 3.6.0-alpha.5 binaries at https://www.dropbox.com/scl/fo/u79134f365jdacqsm0km3/AKMSKB_Fz63WH4hqLkIphuQ?rlkey=bpa9lja4jylkpu9syjfp31rho&dl=0 and the release notes at https://github.com/Duet3D/RepRapFirmware/wiki/Changelog-RRF-3.x-Beta#reprapfirmware-360-alpha5.
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@dc42 I didnt check the exact time , but just under 40 min would be about right for me too.
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@dc42 Mine was actually around the 3.5-4 hour mark for the print. The print I was doing was around 3.75 hours, and it paused with around 15 minutes left. There may have been a delay in the print start too, my machine is a flying gantry so I need to rerun G32 every time the motors shut off, and I may have waited a bit of time for heat soaking since I was printing ASA, so it could've been 4-4.5 hours after the restart.
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@dc42 said in RepRapFirmware 3.6.0-alpha.4+3 available for testing:
I've put the 3.6.0-alpha.5 binaries at https://www.dropbox.com/scl/fo/u79134f365jdacqsm0km3/AKMSKB_Fz63WH4hqLkIphuQ?rlkey=bpa9lja4jylkpu9syjfp31rho&dl=0 and the release notes at https://github.com/Duet3D/RepRapFirmware/wiki/Changelog-RRF-3.x-Beta#reprapfirmware-360-alpha5.
Just ran the initial function test with alpha.5, and the "pause" after each probe move that I mentioned back in July is gone now. Which sure is nice
I've noticed that a bug from earlier (don't remember when) seem to have been reintroduced though, when i push the "bed leveling" button on PD i't don't display any of the messages nested in
bed.g
on the PD, only in DWC.Running the same test print as earlier on alpha.5 now to see if finish without any step timing errors.
And I can also comfirm that it finished the same test print without any issues!
The PA changes is quite segnificant compared to alpha.2 as well. As can be seen in the test prints:
Pressure advance changing every 10mm in these increments:- 0-10mm = PA: 0.045s.
- 10-20mm = PA: 0.025s.
- 20-30mm = PA. 0.01s.
- 30-40mm = PA: 0.0075s.
- 40-50mm = PA: 0.005s.
- 50-60mm = PA: 0s / off.