Strange Behavior , after "Pause" 'Cancel ""print again"
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Duet 3+mini5
DWC RC2
RRP RC2im get a Strange Behavior on bed leveling after "Pause" 'Cancel ""print again"
When the bed tries to do the 3 Point leveling the Z motors seem to be in a low current mode and are skipping steps.
; General preferences
G90 ; send absolute coordinates...
M83 ; ...but relative extruder moves
M550 P"Valkyrie 3030 V001" ; set printer name
M669 K1 ; core xy; Network
M552 S1 ; enable network
M586 P0 S1 ; enable HTTP
M586 P1 S0 ; disable FTP
M586 P2 S0 ; disable Telnet; Drives
M569 P0.0 S1 ; physical drive 0 goes forwardsM569 P0.1 S1
M569 P0.1 S1 ; physical drive 1 goes forwardsM569 P0.1 S1
M569 P0.2 S1 ; physical drive 2 goes forwards ( blown needs replacing)
M569 P0.3 S1 ; physical drive 3 goes forwards (extruder
M569 P0.4 S1 D3 V30 ; physical drive 4 goes forwards D3=stealthchop
M569 P0.5 S0 D3 V30 ; physical drive 5 goes backwards
M569 P0.6 S1 D3 V30 ; physical drive 6 goes forwardsM584 X1 Y0 E3 Z0.4:0.5:0.6 ; set drive mapping FL,FR,RC
M350 X16 Y16 I1 ; configure microstepping with interpolation
M350 Z16 E16 I1
M92 X80.00 Y80.00 Z320.00 E260.00 ; set steps per m
M566 X500.00 Y500.00 Z800.00 E100.00 P1 ; set maximum instantaneous speed changes (mm/min)
M203 X8000.00 Y8000.00 Z1000.00 E400.00 ; set maximum speeds (mm/min)
M201 X1000.00 Y1000.00 Z200.00 E250.00 ; set accelerations (mm/s^2)
M906 X1000 Y1000 Z1000 E1400 I10 ; set motor currents (mA) and motor idle factor in per cent
M84 S20 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; set axis minima "Travel Area"
M208 X270 Y240 Z405 S0 ; set axis maxima "Travel area"; Endstops
M574 X1 S1 P"!io0.in" ; configure switch-type (e.g. microswitch) endstop for low end on X via pin io0.in
M574 Y2 S1 P"!io1.in" ; configure switch-type (e.g. microswitch) endstop for low end on Y via pin io1.in
;M574 Z2 S2 P"!io4.in" ; != invert signal
M574 Z2 S4 ; configure sensorless endstop for high end on Z, 1 = low end, 2 = high end. S4 multipule motors
M671 X-34.4:296:132.5 Y0:0:296 S25 ; leadscrews at front left,front right, rear Center s= max correction factor must be in same order as M584M558 P8 C"!io3.in" H5 F600 T18000 A30 S0.03 ; set Z probe type to unmodulated and the dive height + speeds
G31 P500 Z0.9 ; set Z probe trigger value, offset and trigger height bigger the posative number the closer to the bed
G31 P500 X26 Y6 ; set x,y trigger value, offset and trigger height
M557 X30:270 Y10:250 S40 ; define mesh grid; Heaters
M308 S0 P"temp0" Y"thermistor" T100000 B3950 A"Bed T°C" ; configure sensor 0 as thermistor on pin bedtemp
M950 H0 C"out0" T0 Q10 ; create bed heater output on bedheat and map it to sensor 0
M307 H0 R0.140 K0.103:0.000 D43.19 E1.35 S0.90 B0 ; PDI info for 8mm aluminium bed 700w Heater NTC 100K 3950
M140 H0 ; map heated bed to heater 0
M143 H0 S120 ; set temperature limit for heater 0 to 120C
M308 S1 P"temp1" Y"thermistor" T100000 B4267 A"Extruder T°C" ; configure sensor 1 as thermistor on pin e0temp (104gt2)
M950 H1 C"out1" T1 ; create nozzle heater output on e0heat and map it to sensor 1
M307 H1 R3.435 K0.348:0.274 D6.64 E1.35 S1.00 B0 V23.9 ; disable bang-bang mode for heater and set PWM limit
M143 H1 S280 ; set temperature limit for heater 1 to 280C; Fans
M950 F0 C"out4" Q500 ; create fan 0 on pin fan0 and set its frequency
M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
M950 F1 C"out3" Q500 ; create fan 1 on pin fan1 and set its frequency
M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on; Tools
M563 P0 D0 H1 F0 ; define tool 0
G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C; Custom settings are not defined
M98 P/macros/3zhome;3zhome
M400
M569 P0.4:0.5:0.6 V10
G4 P100
M574 Z2 S4
M906 Z300 ; set motor current
G91 ; relative positioning
G1 H2 Z0.2 F3000 ; power up motors to ensure they are not stalled
G4 P100 ; wait 100ms
M400 ; wait for current moves to finishG4 P200
M915 P0.4:0.5:0.6 S0 H10 F0 R0 ; Configure Z-Axis Stall DetectionG4 P200
G91 ; relative positioning
G1 F4000
G1 H1 Z350 ; Home Z-Axis actuators independently
M400 ; make sure everything has stopped before we make changes
M906 Z600 ; Reset motor current
G90 ; absolute positioning
G92 Z301 ; set position
G91 ; relative positoning
M84 ; Motors off -
@moth4017
It would help if you post the contents of pause.g, cancel.g, stop.g and your start gcode
Use the </> button so that we can easily scroll through the contents. -
; pause.g ; called when a print from SD card is paused ; ; generated by RepRapFirmware Configuration Tool v3.3.10 on Thu Dec 30 2021 11:07:38 GMT+1300 (New Zealand Daylight Time) M83 ; relative extruder moves G1 E-10 F3600 ; retract 10mm of filament G91 ; relative positioning G1 Z5 F360 ; lift Z by 5mm G90 ; absolute positioning G1 X0 Y0 F6000 ; go to X=0 Y=0 ; stop.g ; called when M0 (Stop) is run (e.g. when a print from SD card is cancelled) ; ; generated by RepRapFirmware Configuration Tool v3.3.10 on Thu Dec 30 2021 11:07:38 GMT+1300 (New Zealand Daylight Time) No Cancel.g Start script M104 S[first_layer_temperature] ; set extruder temp M109 S[first_layer_temperature] ; wait for extruder temp G28 ; home all
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@moth4017
I don't see anything out of the ordinary in those files.
Your M569 V parameter seems very low compared to the documentation, but I've never used that so I don't know enough to comment. -
@moth4017 What current are you expecting the steppers to be set to? Your home z seems to leave it set to 600mA (which is significantly lower than the 1000mA initially set in config.g). You might want to try running M906 from the console before your initial print and then after you have hit pause and again after cancel to see what current is set at the various stages.
Not totally sure if it will help but you might also want to reconfigure the stall threshold to be higher after you have completed your homing just in case that is causing problems.
I notice that you also have M84 at the end of your zhome code, this is unusual. What are you expecting it to do?
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@gloomyandy
Hi i have also tried setting current to 1000ma still the same issue.Ill try the M906 later
M84 is at the end of the home Z as i send the bed to Max Z and then turn off the motors , -
I think what's happening is that you're moving the Z axis to the max position and reducing the current. When it tries to move again it's stalling or maybe binding.
Return your motor current to normal before trying to move the axis again and see if it's able to move.
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@phaedrux
Hi when i do "pause print" "cancel" "print again" the bed has remained at the top position so it has not done the sensorless homing at Z max -
@moth4017 said in Strange Behavior , after "Pause" 'Cancel ""print again":
No Cancel.g
Can you create a cancel.g file? Either put in some commands you want to happen when the print is canceled, or leave it blank for it to do nothing. The default cancel behaviour may be your problem.
https://docs.duet3d.com/en/User_manual/Reference/Gcodes#m0-stop-or-unconditional-stop
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i should have done this before sorry
in the console when i press "print again"
i get these error messages
Error: Homing failed
Error: Driver 0.4 error: over temperature shutdown
Error: Driver 0.5 error: over temperature shutdown
Error: Driver 0.4 error: over temperature shutdown
Error: Driver 0.5 error: over temperature shutdown
Warning: Driver 0.4 warning: over temperature warning -
@moth4017 Did you try running M906 so that you can see what current setting the drivers are using when they generate errors?
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M906 pre test X,y,Z 1000ma
after Cancel print
M906Motor current (mA) - X:1000, Y:1000, Z:1000, E:1400, idle factor 10% -
@moth4017 Very odd? Do you always get those driver temperature errors when you have this problem?
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@gloomyandy
Hi Yes , but i can print ok if i send new G code , it only hppend after the above sequency -
@phaedrux
If i add the cancel.g file when pressing "cancel" button the cancel.g file does not run, cancel.g file in system directory;cancel.g M98 P/macros/home_max_Z ; home_max_Z M400 ; make sure everything has stopped before we make changes ;G91 ; relative positioning ;;M915 P0.4:0.5:0.6 S3 F0 R0 ; Configure Z-Axis Stall Detection ;M913 Z80 ; Lower motor current by 50% ;M574 Z2 S4 ; Configure Z-Axis stall detection homing ;G91 ; relative positioning M98 P/macros/sensorless_Z G1 F3000 ; G1 H1 Z350 ; Home Z-Axis actuators independently M400 ; make sure everything has stopped before we make changes M913 Z100 ; Reset motor current G90 ; absolute positioning G92 Z290 ;sensorless_z M915 P0.4:0.5:0.6 S3 F0 R0 ; Configure Z-Axis Stall Detection M906 Z300 ; Lower motor current by 50% M574 Z2 S4 ; Configure Z-Axis stall detection homing M400 ; make sure everything has stopped before we make changes M906 Z1000 ; Reset motor current M400
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Can you share the results of sending M122 and M98 P"config.g" ?
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@phaedrux ```
3/11/2022, 11:01:06 AM M122
=== Diagnostics ===
RepRapFirmware for Duet 3 Mini 5+ version 3.4.0rc2 (2022-02-22 17:07:31) running on Duet 3 Mini5plus WiFi (standalone mode)
Board ID: 3R9YY-6T9RL-D65J0-40KMN-2UW2Z-RHYT0
Used output buffers: 3 of 40 (15 max)
=== RTOS ===
Static ram: 103652
Dynamic ram: 110396 of which 0 recycled
Never used RAM 27592, free system stack 132 words
Tasks: NETWORK(ready,49.2%,228) HEAT(notifyWait,0.1%,356) Move(notifyWait,0.0%,292) CanReceiv(notifyWait,0.0%,942) CanSender(notifyWait,0.0%,356) CanClock(delaying,0.0%,339) TMC(notifyWait,3.6%,114) MAIN(running,44.5%,428) IDLE(ready,0.0%,29) AIN(delaying,2.5%,264), total 100.0%
Owned mutexes: WiFi(NETWORK)
=== Platform ===
Last reset 02:17:44 ago, cause: power up
Last software reset at 2022-03-09 19:21, reason: User, GCodes spinning, available RAM 24040, slot 2
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
MCU revision 3, ADC conversions started 8264987, completed 8264987, timed out 0, errs 0
Step timer max interval 754
MCU temperature: min 28.5, current 30.2, max 32.7
Supply voltage: min 23.8, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Events: 0 queued, 0 completed
Driver 0: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
Driver 1: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
Driver 2: pos 96320, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
Driver 3: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30413, writes 9, timeouts 0, DMA errors 0, CC errors 0
Driver 4: pos 0, standstill, SG min 174, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
Driver 5: pos 0, standstill, SG min 16, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
Driver 6: pos 0, standstill, SG min 26, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
Date/time: 2022-03-11 11:01:05
Cache data hit count 4294967295
Slowest loop: 5.52ms; fastest: 0.13ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 22.5MBytes/sec
SD card longest read time 14.1ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 83, segments created 3, maxWait 624ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 2, completed 2, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty
=== CAN ===
Messages queued 74382, received 0, lost 0, boc 0
Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 18 (min 18), ts 41325/0/0
Tx timeouts 0,0,41324,0,0,33056 last cancelled message type 30 dest 127
=== Network ===
Slowest loop: 16.87ms; fastest: 0.00ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
HTTP sessions: 1 of 8- WiFi -
Network state is active
WiFi module is connected to access point
Failed messages: pending 0, notready 0, noresp 0
WiFi firmware version 1.25
WiFi MAC address f0:08:d1:02:a1:0b
WiFi Vcc 3.34, reset reason Power up
WiFi flash size 2097152, free heap 25512
WiFi IP address 192.168.0.19
WiFi signal strength -49dBm, mode 802.11n, reconnections 0, sleep mode modem
Clock register 00002002
Socket states: 0 0 0 0 0 0 0 0
HTTP is enabled on port 80 FTP is disabled TELNET is disabled
- WiFi -
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@phaedrux
hi any thourghts? -
@moth4017 said in Strange Behavior , after "Pause" 'Cancel ""print again":
@phaedrux
If i add the cancel.g file when pressing "cancel" button the cancel.g file does not run, cancel.g file in system directory;cancel.g M98 P/macros/home_max_Z ; home_max_Z M400 ; make sure everything has stopped before we make changes ;G91 ; relative positioning ;;M915 P0.4:0.5:0.6 S3 F0 R0 ; Configure Z-Axis Stall Detection ;M913 Z80 ; Lower motor current by 50% ;M574 Z2 S4 ; Configure Z-Axis stall detection homing ;G91 ; relative positioning M98 P/macros/sensorless_Z G1 F3000 ; G1 H1 Z350 ; Home Z-Axis actuators independently M400 ; make sure everything has stopped before we make changes M913 Z100 ; Reset motor current G90 ; absolute positioning G92 Z290 ;sensorless_z M915 P0.4:0.5:0.6 S3 F0 R0 ; Configure Z-Axis Stall Detection M906 Z300 ; Lower motor current by 50% M574 Z2 S4 ; Configure Z-Axis stall detection homing M400 ; make sure everything has stopped before we make changes M906 Z1000 ; Reset motor current M400
Can you try a simplified cancel.g? Maybe just a G28 XY
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;cancel.g
G28 X YThe console displayed this after cancel print:-
M0
Printing paused at X128.9 Y78.9 Z0.3
Cancelled printing file 0:/gcodes/shark-v2-0-a_0.35mm_PLA__2h32m.gcode, print time was 0h 5mthe Cancel.g file didnt run, so i put "G28 X Y" in the command line , this ran perfectly , but then i got this error in the console , only happens when i do the "Cancel"
3/16/2022, 7:56:33 PM Error: Driver 0.4 error: over temperature shutdown
3/16/2022, 7:56:33 PM Emergency stop, attemping to reconnect...
3/16/2022, 7:56:31 PM Error: Driver 0.6 error: over temperature shutdown
3/16/2022, 7:56:31 PM Error: Driver 0.5 error: over temperature shutdown
3/16/2022, 7:56:30 PM Error: Driver 0.4 error: over temperature shutdown