need Guru on duet 3 mini5 using stall guard/sensor less homing
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The 2660s do StallGuard2 in SpreadCycle, the 2209s do StallGuard4 in StealthChop. They work differently, so it's not a super big surprise that they need specific tuning.
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hi any thoughts on how i can track the homing issues ?
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No more Gurus out there playing with the Duet 3 mini5 tmc2209
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@moth4017 Guru meditation …
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@infiniteloop tried for 6 months ... its not working . but ever hopeful
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@moth4017
this is my config and it works nice; Configuration file for Duet 3 Mini 5+ (firmware version 3.3) ; executed by the firmware on start-up ; ; generated by RepRapFirmware Configuration Tool v3.3.10 on Mon May 02 2022 10:42:59 GMT+0200 (Mitteleuropäische Sommerzeit) ; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Bear 2.1 Duet3d mini5+" ; set printer name M918 P1 E4 F2000000 ; configure direct-connect display ; Network M552 P192.168.178.148 S1 ; enable network and set IP address M553 P255.255.255.0 ; set netmask M554 P192.168.178.1 ; set gateway M586 P0 S1 C"*" ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet ; Drives M569 P0.0 S0 D3 V100 ; x physical drive 0.0 goes forwards M569 P0.1 S1 D3 V100 ; y physical drive 0.1 goes forwards ;M569 P0.0 S0 D3 V40 ; x physical drive 0.0 goes forwards ;M569 P0.1 S1 D3 V40 ; y physical drive 0.1 goes forwards M569 P0.2 S0 D3 V0 ; z1 physical drive 0.2 goes forwards M569 P0.3 S0 D3 V0 ; z2 physical drive 0.3 goes forwards M569 P0.4 S1 D3 ; e physical drive 0.4 goes forwards was d2 M584 X0.0 Y0.1 Z0.2:0.3 E0.4 ; set drive mapping ; z axis compensation M671 X-36.5:289.3 Y105:105 S1.75 M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation M92 X100.00 Y100.00 Z400.00 E398.00 ; set steps per mm ;M566 X360.0 Y360.0 Z360.0 E360.0 ; set maximum instantaneous speed changes (mm/min) Worked with vibrations ;M566 X360.0 Y360.0 Z360.0 E360.0 ; set maximum instantaneous speed changes (mm/min) M566 X900.0 Y900.0 Z60.0 E3000.0 P1 ; set maximum instantaneous speed changes (mm/min) ;M566 X900 Y900 Z60 E3000 P1 M203 X9000.00 Y9000.00 Z1800.00 E4800.00 ; set maximum speeds (mm/min) ;M203 X15000.00 Y15000.00 Z1800.00 E4800.00 ; set maximum speeds (mm/min) M201 X2500.00 Y2500.00 Z100.00 E10000.00 ; set accelerations (mm/s^2) ;M201 X8000.00 Y8000.00 Z100.00 E10000.00 ; set accelerations (mm/s^2) M203 X9000 Y9000 Z600 E20000 ; Sets the maximum feedrates that your machine can do in mm/min ;M203 X15000 Y15000 Z600 E20000 ; Sets the maximum feedrates that your machine can do in mm/min ;M566 X360.0 Y360.0 Z360.0 E360.0 ; set maximum instantaneous speed changes (mm/min) ;M566 X520.0 Y520.0 Z360.0 E360.0 ; set maximum instantaneous speed changes (mm/min) ;M203 X12000.00 Y12000.00 Z1800.00 E4800.00 ; set maximum speeds (mm/min) ;M201 X2500.00 Y2500.00 Z100.00 E10000.00 ; set accelerations (mm/s^2) ;M201 X3500.00 Y3500.00 Z250.00 E10000.00 ;M201 X4500.00 Y4500.00 Z250.00 E10000.00 ;M906 X920 Y990 Z800 E1050 I100 ; set motor currents (mA) and motor idle factor in per cent M906 X920 Y1050 Z800 E1050 I100 ; set motor currents (mA) and motor idle factor in per cent M564 H0 ; allow unhomed movement M84 S30 ; Set idle timeout ; Axis Limits M208 X0 Y-4 Z0 S1 ; set axis minima M208 X250 Y210 Z200 S0 ; set axis maxima ; Endstops M574 X1 S3 ; configure sensorless endstop for low end on X M574 Y1 S3 ; configure sensorless endstop for low end on Y M574 Z1 S2 ; configure Z-probe endstop for low end on Z M915 X S30 H150 R0 ;M915 Y S30 H150 R0 M915 Y S65 H150 R0 ; Z-Probe ;M558 P1 C"io3.in+io3.out" H5 F120 T6000 ; set Z probe type to unmodulated and the dive height + speeds ;G31 P500 X0 Y0 Z2.5 ; set Z probe trigger value, offset and trigger height ;M557 X15:215 Y11:195 S20 ; define mesh grid ; Z-Probe PINDA M574 Z1 S2 ; Above at EndstopsSet endstops controlled by probe ;M558 P5 C"io3.in" I1 H0.7 F1000 T6000 A20 S0.005 ; PINDA M558 P5 C"io3.in" I1 H1.0 F1000 T8000 A20 S0.005 ; PINDA H dive height old M558 P5 C"io3.in" I1 H1.4 F1000 T8000 A20 S0.005 ; PINDA H dive height ;M558 P5 C"io3.in" I1 H1 F1000 T6000 A20 ; PINDA ;M558 P5 C"io3.in" I1 H1.5 F600 T8000 A20 S0.03 ; PINDA M308 S2 P"temp2" A"PINDA" Y"thermistor" T100000 B3950 ;G31 P1000 X23 Y5 Z0.837 ; PEI Sheet Offset C0.0010 S20 H2 original ;G31 P1000 X23 Y5 Z0.870 ; PEI Sheet Offset C0.0010 S20 H2 ;G31 P1000 X23 Y5 Z0.855 ; PEI Sheet Offset C0.0010 S20 H2 ;G31 P1000 X23 Y5 Z1.315 ; Textured Sheet Offset ;G31 P500 X23 Y5 Z0.630 ;trigger height Octoprint sheet ;G31 P1000 X23 Y12 Z1.130 ;trigger height Octoprint sheet ;G31 P1000 X23 Y5 Z0.738 S21 H2 T0.02 ; Nozzle offset - Powder Coated Sheet with temperature compensation (0.02mm/°C) ;G31 P1000 X23 Y5 Z1.130 S21 H2 T0.02 ; Nozzle offset - Zirflex. Powder Coated Sheet with temperature compensation (0.02mm/°C) ;G31 P1000 X23 Y5 Z1.06 S21 H2 T0.02 ; Nozzle offset - Satin Powder Coated Sheet with temperature compensation (0.02mm/°C) ;M557 X24:221 Y10:195 P3 ; Define mesh grid M557 X36:244 Y14:208 P5 ; Define mesh grid ;M557 X12:220 Y5:197 P3 ; Define mesh grid ; ##### Z-Probe Settings for PINDA 2 ;M558 P5 C"io2.in" I1 H1 F1000 T6000 A3 ; Prusa PindaV2 Endstop ;M308 S2 P"temp2" A"Pinda V2" Y"thermistor" T100000 B3950 ; Prusa PindaV2 Thermistor M376 H5 ; Fade height 5mm ; Heaters M308 S0 P"temp0" A"MK52" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0 M307 H0 B0 S1.00 R0.22 ; disable bang-bang mode for the bed heater and set PWM limit 21s for 5 degrees M140 H0 ; map heated bed to heater 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M308 S1 P"temp1" A"Volcano" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin temp1 M950 H1 C"out2" T1 ; create nozzle heater output on out2 and map it to sensor 1 M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit M143 H1 S280 ; set temperature limit for heater 1 to 280C ; Fans M950 F0 C"out5" Q100 ; create fan 0 on pin out3 and set its frequency M106 P0 C"Part Cooling" S0 H-1 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"out6" Q500 ; create fan 1 on pin out4 and set its frequency M106 P1 C"Revo Fan" S255 H1 T45 ; set fan 1 value. Thermostatic control is turned on ; Tools M563 P0 D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined M556 S100 X0,586 ; Miscellaneous M501 ; load saved parameters from non-volatile memory T0 ; select first tool ; Default config.g template for DuetPi ; Replace this with a proper configuration file (e.g from https://configtool.reprapfirmware.org) ; Display initial welcome message ;M291 P"Please go to <a href=""https://www.duet3d.com/StartHere"" target=""_blank"">this</a> page for further instructions on how to set it up." R"Welcome to your new Duet 3!" S1 T0 M98 P"mksmini12864.g" M98 P"/sys/surface.g" ;G4 S30 ;M999
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@danielkrah
Hi are you using sensor less homing on your Z access? -
@moth4017 oh you're asking on sensorless for Z? That's quite likely not going to work since unless you're taking special precautions a) you can't move the Z fast enough b) your print head has to be super rigid so it doesn't just flex when it hits the print bed c) you'll need a rigid print bed that doesn't care about getting hit with the weight of the full gantry.
And even then, the lack of precision on sensorless homing really doesn't make it suitable for Z.
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@oliof Hi i can move my Z very fast at 10000mm/s if i want too but not recommended my Z axis is on 4:1 gear box belt driven so speed not an issue. Im not homing at the print head but at the base of the printer against end stops.
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@moth4017 the best way forward is still to add two microswitches there. If you really insist, we'd need to see some pictures of the setup and your config.g and homez.g
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@oliof hi set up is 3 belt drives config and homing files at stat of thread.
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- H parameter in M915 should be set to the steps/mm for the Z axis which seems to be 320?
- lines 19/23 in home_max_z is probably supposed to be a G4 call, not a G1 call.
- Your M915s may need to have
R0
rather thanR1
(at least that's working for me). - you could replace the acceleration changes (line 32 etc.) by defining M201.1 in config.g with the special move accelerations.
- line 41 should not be required.
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Thanks for the input , tried all of your suggestions
changing the H value didnt seem to have much impact
changed the G1 to G4 ( my mistake )
R0 and R1 did try it but it should not make a difference
M201.1 it thought this had fixed it but on the 14th try failed to move front left stepper
will try tweeking a few values to see if i can make it more reliable -
@moth4017 since your Z steppers are geared, you may run into issues there, so the H value might need to be adjusted accordingly
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@oliof
i have thought about the gearing but the stepper motor is still doing the same amount of steps , but the back EMF generated may happen sooner as there is more torque required, so maybe thats why the M201.1 was a little more reliable -
@moth4017 - whats not working ?
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Hi after a print is finished i send the Build plate to the bottom of the printer (core xy ) i have 3 Z motors belt driven.
when the bed is give the instruction to go to bed max ( gcode above) one or 2 of the motors will not be driven intermittently , sometimes this causes the Bed to fall off not ideal ..
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that sounds like your mechanical system may have binding and is only marginally related to stall detection ... unless the binding is strong enough to trigger stall detection.
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the belts and the gearbox's are very smooth running, i have built printer with ACME threads and these were very smooth but i think the belts and gear boxes could be as good or better.
Keep coming up with things i may have forgot.
did more testing tonight the M201.1 has defiantly made an improvement, played around with the H values did not seem to have any major effect other that a bigger/louder stopping noise until i went too far and didnt stall at all.
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more testing
drive 0 =Y
drive 1 =X
Drive 4,5,6 = Z FL FR RCstill getting stall warnings is this normal?
6/26/2022, 10:19:31 AM === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.4.1 (2022-06-01 21:06:56) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: 3R9YY-6T9RL-D65J0-40KMN-2UW2Z-RHYT0 Used output buffers: 2 of 40 (38 max) === RTOS === Static ram: 103684 Dynamic ram: 111176 of which 24 recycled Never used RAM 23540, free system stack 128 words Tasks: NETWORK(ready,18.0%,238) HEAT(notifyWait,0.0%,326) Move(notifyWait,0.0%,267) CanReceiv(notifyWait,0.0%,942) CanSender(notifyWait,0.0%,356) CanClock(delaying,0.0%,337) TMC(delaying,1.3%,79) MAIN(running,79.8%,388) IDLE(ready,0.0%,29) AIN(delaying,0.8%,264), total 100.0% Owned mutexes: WiFi(NETWORK) File(MAIN) === Platform === Last reset 00:06:27 ago, cause: power up Last software reset at 2022-06-25 20:48, reason: User, GCodes spinning, available RAM 23540, slot 1 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 MCU revision 3, ADC conversions started 387552, completed 387551, timed out 0, errs 0 Step timer max interval 752 MCU temperature: min 27.6, current 28.7, max 28.9 Supply voltage: min 23.6, current 23.8, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/0, heap memory allocated/used/recyclable 2048/1206/1206, gc cycles 0 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 43, reads 5457, writes 17, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 42, reads 5458, writes 16, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 5474, writes 0, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 2, read errors 0, write errors 0, ifcnt 12, reads 5474, writes 1, timeouts 0, DMA errors 0, CC errors 0 Driver 4: ok, SG min 0, read errors 0, write errors 0, ifcnt 34, reads 5462, writes 12, timeouts 0, DMA errors 0, CC errors 0 Driver 5: ok, SG min 0, read errors 0, write errors 0, ifcnt 34, reads 5462, writes 12, timeouts 0, DMA errors 0, CC errors 0 Driver 6: ok, SG min 0, read errors 0, write errors 0, ifcnt 33, reads 5462, writes 12, timeouts 0, DMA errors 0, CC errors 0 Date/time: 2022-06-26 10:19:29 Cache data hit count 678579454 Slowest loop: 187.57ms; fastest: 0.07ms === Storage === Free file entries: 6 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 0.8ms, write time 0.0ms, max retries 0 === Move === DMs created 83, segments created 18, maxWait 23687ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 24, completed 23, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters 2 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.2 Heater 1 is on, I-accum = 0.3 === GCodes === Segments left: 0 Movement lock held by File HTTP is doing "M290 R1 Z-0.05" in state(s) 0 Telnet is idle in state(s) 0 File is ready with "M122" in state(s) 0 0 15, running macro USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 S50 " in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty === CAN === Messages queued 542, received 0, lost 0, boc 0 Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 18 (min 18), ts 301/0/0 Tx timeouts 0,0,301,0,0,241 last cancelled message type 30 dest 127 === Network === Slowest loop: 201.88ms; fastest: 0.08ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions HTTP sessions: 1 of 8 - WiFi - Network state is active WiFi module is connected to access point Failed messages: pending 0, notready 0, noresp 3 WiFi firmware version 1.25 WiFi MAC address f0:08:d1:02:a1:0b WiFi Vcc 3.34, reset reason Power up WiFi flash size 2097152, free heap 27088 WiFi IP address 192.168.0.19 WiFi signal strength -61dBm, mode 802.11n, reconnections 0, sleep mode modem Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0 3PL Drive 0 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 440 Drive 1 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 600 Drive 4 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 964 Drive 5 runs in reverse, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 576 Drive 6 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 216 6/26/2022, 10:19:07 AM Valkyrie OK : Voltage OK : 23.9 6/26/2022, 10:19:05 AM Drive 0 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 1011 Drive 1 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 67 home Z.g 6/26/2022, 10:19:03 AM Warning: Driver 0 stalled at Z height 300.10 Drive 0 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 25, pwmScaleAuto 3, pwmOfsAuto 80, pwmGradAuto 18, pos 306 Drive 1 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 24, pwmScaleAuto 2, pwmOfsAuto 72, pwmGradAuto 19, pos 985 after revert back 6/26/2022, 10:19:02 AM Drive 0 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 23, pwmScaleAuto 0, pwmOfsAuto 78, pwmGradAuto 17, pos 344 Drive 1 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 20, pwmScaleAuto 0, pwmOfsAuto 74, pwmGradAuto 15, pos 1016 home x 6/26/2022, 10:19:02 AM Drive 0 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 866 Drive 1 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 95 start Drive 0 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 866 Drive 1 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 95 stall detection setup lower motor current 6/26/2022, 10:19:00 AM Drive 0 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 18, pwmScaleAuto 0, pwmOfsAuto 67, pwmGradAuto 19, pos 600 Drive 1 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 20, pwmScaleAuto 0, pwmOfsAuto 73, pwmGradAuto 17, pos 248 after revert back 6/26/2022, 10:18:59 AM Warning: Driver 0 stalled at Z height 300.10 6/26/2022, 10:18:56 AM lower motor current Drive 0 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 18, pwmScaleAuto 0, pwmOfsAuto 72, pwmGradAuto 15, pos 504 Drive 1 runs forwards, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 10 (937.5 mm/sec), pwmScaleSum 21, pwmScaleAuto 0, pwmOfsAuto 73, pwmGradAuto 16, pos 344 Home Y 6/26/2022, 10:18:55 AM M32 "0:/gcodes/Body50_0.2mm_PLA__1h44m.gcode" File 0:/gcodes/Body50_0.2mm_PLA__1h44m.gcode selected for printing Home All.g Home Y Drive 0 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 504 Drive 1 runs forwards, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 88 stall detection setup 6/26/2022, 10:18:38 AM after revert back