Error: bad Command XXX W/RRF 3.2 and leveling issue
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@martin7404 Instead of two bearings, what about a option to upgrade to the wide series, mgw9h. This should reduce the tilt, and would result in less binding then two bearings mounted on different planes would.
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@3DPrintingWorld said in Error: bad Command XXX W/RRF 3.2 and leveling issue:
mgw9h
Yes , but you have to switch to 4020 profile for the X and the mass would not be less
I took a look at hiwin pdf's . So LDO rails must light clearance type ZF (4 to 10 microns clearence between block adn rail) so 0.06-0.07 mm on 25 mm cantilever seems normal too. Maybe we can switch to light to slight preload blocks -
@martin7404 Why would we have to switch to a 4020? I have not placed it in the model yet but I think it would fit on the 2020 just fine. As you say a preload would be an improvement too, especially considering there is only a single bearing. It would probably will have to get a genuine Hiwini though for a preload option.
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Sorry I missed that 09MGW is a single row of bolts.
MGW is better I agree X momentum is about 3 times bigger -
@Phaedrux There really is not much I can omit from the config as most of it is needed for homing. I can remove heaters, fans, and filament sensors but I don't see how that is going to help.
Have you seen any documentation to recover from the firmware being deleted?
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@Phaedrux neverminded, I found fallback procedure 3.
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@3DPrintingWorld more likely due to the magnetic mat not flat within 0.15 mm. I tried pushing the X head lightly with my finger during G32, no diference
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So found a major problem with Muldex and PRF 3.2
Started a print with T1 ( right , not main extruder) and all of suden the machine is printing in thin air , a few mm up, looked at paneldue and it shows of Z layer + my T1 offset - Z+2.85. Canceled the print.
In manual when I entrer T0 or T1 in the console , both heads come to exact position , measured with 10.5 mm steel gauge .
I do not understan what is hapening . With PRF 3.0 it was printing like a charm
Here is my configG90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Muldex" ; set printer name ; Network M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet ; Drives M569 P0 S0 ; X physical drive 0 goes backwards M569 P1 S0 ; Y right physical drive 1 goes backwards M569 P2 S1 ; Y left physical drive 2 goes forwards M569 P3 S1 ; U physical drive 3 goes forwards M569 P4 S1 ; E1 physical drive 4 goes backwards M569 P5 S1 ; Z left physical drive 5 goes backwards M569 P6 S1 ; Z center physical drive 6 goes backwards M569 P7 S0 ; Z right physical drive 7 goes forwards M569 P8 S1 ; E2 physical drive 8 goes forwards M584 X0 Y1:2 U3 Z5:6:7 E4:8 ; set drive mapping M350 X16 U16 Y16 Z16 E16:16 I1 ; configure microstepping with interpolation M92 X199.7 U200 Y199.8:199.8 Z799.2:799.2:799.2 E813.07:830.00 ; set steps per mm (1760nimble) M566 X1000.00 U1000.00 Y1000.00:1000.00 Z80.00:80.00:80.00 E100.00:100.00 ; set maximum instantaneous speed changes (mm/min)(Nimble 40) M203 X12000.00 U12000.00 Y12000.00:12000.00 Z1000.00:1000.00:1000.00 E4200.00:4200.00 ; set maximum speeds (mm/min) M201 X1310.00 U1310.00 Y1310.00:1310.00 Z35.00:35.00:35.00 E800.00:800.00 ; set accelerations (mm/s^2)(500)(Nimble 120) M906 X900 U900 Y900:900 Z900:900:900 E1000:1000 I30 ; set motor currents (mA) and motor idle factor in per cent(Nimble 500) M84 S120 ; Set idle timeout ; Axis Limits M208 X-18 Y0 U40 Z0 S1 ; set axis min - adjust X to align nozzle M208 X350 U422.7 Y333 Z300 S0 ; set axis max M669 K0 Y1:-1:0:1 ; select Markforged Kinematics Y to react with X and U ; Endstops M574 X1 S1 P"xstop" ;X axis active high endstop switch M574 Y2 S1 P"ystop+e1stop" ;Y Double max active high endstop switch ;M574 Y1 S4 ; configure sensorless endstop for low end on Y M574 U2 S1 P"e0stop" ;U axis active high endstop switch ;M574 Z2 S4 ;Stall Detection(no used) ;M574 Y1 S4 ; Y axis stall detection ;M915 P1:9 S3 F1 R0 ; Y axis stall detection ; Z-Probe M671 X-20.6:200:420.6 Y14.3:333.3:14.3 S10 ; Locations left, center, right M950 S0 C"duex.e6heat" ; create servo pin 0 for BLTouch M558 P9 C"zprobe.in+zprobe.mod" H8 F600 A1 T12000 ; set Z probe type to bltouch and the dive height + speeds G31 P25 X-29 Y0 Z1.42 ; set Z probe trigger value, offset and trigger height(lower number farther away)1.8build 1.7glass M557 X10:320 Y20:290 S60 ; probe from X=10 to 390, Y=10 to 290mm with a mesh spacing of 20mm ; Heaters M308 S0 P"bedtemp" Y"thermistor" T100000 B4534 C9.565227e-8 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M307 H0 B0 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 M308 S1 P"e0temp" Y"thermistor" T100000 B4725 C0 R4700 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H1 S280 ; set temperature limit for heater 1 to 280C M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit M308 S2 P"e1temp" Y"thermistor" T100000 B4725 C0 R4700 ; configure sensor 2 as thermistor on pin e1temp M950 H2 C"e1heat" T2 ; create nozzle heater output on e1heat and map it to sensor 2 M143 H2 S280 ; set temperature limit for heater 2 to 280C M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Fans M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency M106 P2 S0 H-1 ; set fan 2 value. Thermostatic control is turned off M950 F3 C"duex.fan8" Q500 ; create fan 3 on pin duex.fan8 and set its frequency M106 P3 S1 H2 T45 ; set fan 3 value. Thermostatic control is turned on ; LEDs M950 F4 C"duex.fan6" ;Q500 ; create LED 4 on pin duex.fan6 and set its frequency M106 P4 S128 H-1 ; set LED 4 value. Thermostatic control is turned OFF M950 F5 C"duex.fan7" ;Q500 ; create LED 5 on pin duex.fan7 and set its frequency M106 P5 S128 H-1 ; set LED 5 value. Thermostatic control is turned OFF ; Tools M563 P0 D0 H1 F0 S"Left" ; define tool 0 Left G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets y was .45 G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C M563 P1 D1 H2 X3 F2 S"Right" ; define tool 1 Right G10 P1 X0 Y0 Z2.55 ; set tool 1 axis offsets - adjust Y to alignn nozzle G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C M563 P2 D0:1 H1:2 X0:3 F0:2 S"Copy" ; define tool 2 Copy G10 P2 X90 Y0 U-90 S0 R0 ; set tool 2 axis offsets (WAS 105) M567 P2 E1:1 M568 P2 S1 ; turn on mixing for tool 2 ; set mix ratio 100% on both extruders ;G10 L1 P1 X0.0 Y0.0 Z2.55 M501 ; Record M593 F66.6 M575 P1 S1 B57600 ;Panel due ;G92 Z150 ;G91 ;G1 Z0.1 f100 ;G90
There is more , while printing in the air I pushed baybysteping up to - 2.5 , as a result the Z on panel due become almost +6 mm and the nozzle was still printing in air
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@martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:
It's because you have a offset of "Z2.55" On the U axis tool for some reason.
M563 P1 D1 H2 X3 F2 S"Right" ; define tool 1 Right G10 P1 X0 Y0 Z2.55 ; set tool 1 axis offsets - adjust Y to alignn nozzle G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C
Not sure why it was the same when you tried it manually.
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My left tool head is V6 and is 2.55 mm different from the copperhead
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Just revert back to PRG 3.1.1 and it is the same
Start print the head (T1) prints on Z 2.55 on the screen of DWC and is about 2.55 in the air. So just like there are 2 offsets applied one over the other,
One of them is just like you made it in the slicer.
One more thing using babysteps it changes the dimension on the DWC screen If I do - babysteps the screen Z goes up . It is the same with PRF3.1.1 and 3.2 -
@martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:
My left tool head is V6 and is 2.55 mm different from the copperhead
oh, sorry I forgot that you had one V6.
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@martin7404 Can you verify in the G-code that they should be printing at the same height?
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Here is the beginning of the code
; generated by PrusaSlicer 2.3.0+win64 on 2021-02-17 at 12:32:24 UTC ; ; external perimeters extrusion width = 0.45mm ; perimeters extrusion width = 0.45mm ; infill extrusion width = 0.45mm ; solid infill extrusion width = 0.45mm ; top infill extrusion width = 0.40mm ; first layer extrusion width = 0.42mm M107 ;TYPE:Custom M140 S90 ; set bed temp G10 P1 R240 S260 ; set standby and active temps for tool 1 T1 P0 ; shortly activate tool 1 so that it goes to standby temp afterwards T-1 P0 ; deselect any tool G28 Y ; home Y axis G28 XU ; home X and U axis M190 S90 ; wait for bed temp G28 Z ; bed probing and leveling G29 S1 ; call saved bed shape map T1 ; select tool 1 M116 P1 ; wait tool 1 active temp G1 X135 Y-3 F8000 ; move above prime line start position G1 Z0.25 ; get close to bed G92 E0.0 ; reset extruder position G1 X235 E22 F1000.0 ; prime line with first tool G92 E0.0 ; reset extruder position M221 S95 D1 G21 ; set units to millimeters G90 ; use absolute coordinates M83 ; use relative distances for extrusion ;LAYER_CHANGE ;Z:0.3 ;HEIGHT:0.3 G1 Z0.300 F10800.000 G1 E-0.60000 F2400.000 G1 Z0.700 F10800.000 G1 X198.287 Y128.383 G1 Z0.300 G1 E0.60000 F2400.000 M204 S1000 ;TYPE:Skirt ;WIDTH:0.42 G1 F1124.798 G1 X199.050 Y127.844 E0.04350 G1 X199.959 Y127.645 E0.04333 G1 X240.004 Y127.644 E1.86499 G1 X240.884 Y127.817 E0.04177 G1 X241.633 Y128.303 E0.04160
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@martin7404 Should the offset be negative instead of positive? Sorry I'm not sure which one is longer, or shorter.
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I am not quite sure, but in manual, I do tool change and on 10.5 Z my gauge is spot on. I tested the right extruder month ago, but with changing the system ofset. When negative it is not right. Looking at e3d tool changer it is negative, you might be right
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@3DPrintingWorld The V6 is shorter, otherwise, I would make them equal in Z. I hate that thing with tools and the Z shown on the screen since old Fanuc millnig CNC controls. Exactly why for tooling work I do not use length compensation and just switch the WCS (G54 , G55 etc) for each tool
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@martin7404 Yeah, I think you would have a hard time trying to find 2.5mm to remove from the height. When I switched from the nimble to the BMG I really fought to keep the extruder as low to the bearing as I could.
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@3DPrintingWorld The problem for me is that there is no info how duet handles tool offsets I made it successfully on Dual lifting hotends but it was on PRF 2.5 and the moving extruder was longer
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@martin7404 According to this you change the offset of T1. This tells me that the number can be positive or negative because otherwise you would have to modify T0 offset if the number was negative.